ASN Wikibase Occurrence # 356736
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 4 September 1996 |
Time: | 20:25 LT |
Type: | Cessna 425 |
Owner/operator: | Private |
Registration: | N425WB |
MSN: | 425-0028 |
Year of manufacture: | 1981 |
Total airframe hrs: | 3794 hours |
Engine model: | P&W PT6-135 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Auburn, CA -
United States of America
|
Phase: | Landing |
Nature: | Executive |
Departure airport: | Everett, WA (KPAE) |
Destination airport: | (KAUN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, at the conclusion of a 2.5 hour cross-country flight, he landed without difficulty within the first 1/4 of runway 07, which was 3,100 long by 60 feet wide. He applied full reverse thrust, and then he discontinued its use as the airplane slowed and approached the last 1/3 of the runway. The pilot then depressed the brake peddles. The right peddle 'went to the floor,' and the airplane veered left. About 3/4 of the way down the runway, the pilot feathered the right propeller and applied power to the left engine. Despite these efforts, the airplane continued veering toward the left, and it eventually went into a ditch collapsing the nose gear. During a subsequent examination of the airplane's brake system, the right gear brake pads and disc were found in good (serviceable) condition. However, the O-rings in the brake housing had a distorted shape. When the brake system was pressurized, hydraulic fluid leaked past the O-rings. New O-rings were installed in the right brake assembly, and it was pressurized. No leaks were noted, and the brake system then appeared airworthy. The airplane was maintained on an approved inspection program, and it had been inspected about 110 hours before the accident flight.
Probable Cause: failure of the right brake system (master cylinder O-ring seal). Factors relating to the accident were: the narrow runway, and the presence of a ditch adjacent to the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX96LA328 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB LAX96LA328
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 10:23 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation