ASN Wikibase Occurrence # 35685
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Date: | Tuesday 28 March 1995 |
Time: | 09:20 LT |
Type: | Cessna 172N |
Owner/operator: | Johnson, R. Verle |
Registration: | N2196E |
MSN: | 17271184 |
Year of manufacture: | 1978 |
Total airframe hrs: | 1943 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 2 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Venice, FL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | Punta Gorda, FL (PGD |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT WAS BRIEFED ABOUT 2 HOURS BEFORE TAKEOFF THAT FOG EXISTED NEAR HIS DESTINATION AIRPORT AND TO CALL BACK FOR A WEATHER UPDATE; HE DID NOT. THE PILOT TOLD THE SURVIVORS BEFORE TAKEOFF 'WE'RE A LITTLE OVER WEIGHT, I'M NOT SURE IF WE'RE GOING TO TAKEOFF.' AFTER TAKEOFF THE FLIGHT WAS OBSERVED TO FLY INTO THE FOG SEVERAL TIMES AND THE AIRPLANE FLEW OVER THE AIRPORT 3 TIMES. AFTER THE THIRD PASS THE PILOT TOLD THE SURVIVORS HE WAS GOING TO LAND ON THE NEXT ATTEMPT. THE FLIGHT AGAIN ENTERED THE FOG FOR A LONGER DURATION THIS TIME AND THE SURVIVORS STATED THAT THEY AGAIN HEARD THE STALL WARNING HORN. THE PILOT APPLIED POWER BUT THE AIRPLANE DESCENDED NOSE AND RIGHT WING LOW. THE AIRPLANE IMPACTED THE WATER ABOUT 5-10 SECONDS AFTER THE STALL WARNING HORN WAS HEARD. WITNESSES AND THE SURVIVORS STATED THAT THE ENGINE SOUNDED NORMAL THE ENTIRE FLIGHT. THE AIRPLANE WAS RECOVERED AND EXAMINATION OF THE FLIGHT CONTROLS REVEALED NO EVIDENCE OF PREIMPACT FAILURE OR MALFUNCTION. THE PILOT'S MEDICAL CERTIFICATE EXPIRED AFTER DECEMBER 31, 1990, AND HE WAS NOT INSTRUMENT RATED.
Probable Cause: INTENTIONAL VFR FLIGHT INTO IMC BY THE PILOT-IN-COMMAND, FAILURE OF THE PILOT TO MAINTAIN AIRCRAFT CONTROL, SPATIAL DISORIENTATION, AND ALTITUDE INADEQUATE FOR RECOVERY FOLLOWING THE IN FLIGHT LOSS OF CONTROL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA95FA094 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB MIA95FA094
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 16:05 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, Category, Accident report] |
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