ASN Wikibase Occurrence # 356996
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Date: | Monday 22 July 1996 |
Time: | 19:30 LT |
Type: | Cessna 172K |
Owner/operator: | T.r. Pegasus |
Registration: | N46700 |
MSN: | 17257436 |
Total airframe hrs: | 3281 hours |
Engine model: | Lycoming O-320E2D |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | West Milford, NJ -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (4N1) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:An airline transport pilot, occuping the right front seat of the airplane, was performing takeoffs and landings to runway 24, with a passenger in the left front seat, and another passenger seated in the rear seat. The airplane landed long, with full flaps, and the pilot decided to abort the landing (go around). The pilot stated that the airplane failed to accelerate, and he retracted 'some' of the flaps. During the aborted landing, the airplane struck trees about 300 feet south of the runway. Examination of the airplane revealed no pre-impact failure of the engine, airframe or flight controls, and the flaps were at approximately 10 degrees. The pilot listed the runway length as 4,000 feet; however, the actual length was 2,734 feet. The Owner's Manual listed a ground roll landing distance of 520 feet for a maximum gross weight airplane under standard conditions, and total takeoff distance of 1,525 feet to clear a 50 foot obstacle.
Probable Cause: the pilot's failure in attaining the proper touchdown point, and his delay in initiating a go-around (aborted landing).
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC96LA154 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB NYC96LA154
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 13:06 |
ASN Update Bot |
Added |
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