Accident Piper PA-23-250 N6819Y,
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ASN Wikibase Occurrence # 357032
 
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Date:Wednesday 17 July 1996
Time:15:35 LT
Type:Silhouette image of generic PA27 model; specific model in this crash may look slightly different    
Piper PA-23-250
Owner/operator:L C E Inc.
Registration: N6819Y
MSN: 27-4158
Year of manufacture:1969
Total airframe hrs:4691 hours
Engine model:Lycoming TIO-540-C1A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:St Petersburg, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:(KSPG)
Destination airport:Watchula, FL (FD06)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot departed on a flight on the day after an annual inspection had been completed. After departing, he reported, the right engine was 'running rough.' The control tower cleared him for an emergency landing back at the airport. While returing, the pilot was unable to maintain altitude, and the flight impacted water about 1 mile south of the airport. According to the pilot's statement, he was flying westbound over water, when the right engine 'stopped.' He stated that he 'secured' the right engine, and about 1 minute later, the left engine 'stopped.' He 'secured' the left engine, and the airplane 'hit water.' The pilot stated that he was in the air about 15 minutes when the loss of engine power occurred. Examination of the right engine revealed, there was rusty water in the sediment bowl at the fire wall; rusty water and contamination were also found in the respective fuel servo screen. The left engine sediment bowl was found dry; the respective fuel servo screen was found with rust stains and contamination with 'trash' in the screen. The fuel selector valves operated without any discrepancies. No preimpact mechanical discrepancy was found with either engine.

Probable Cause: a loss of engine power due to fuel contamination, which resulted in a forced landing (ditching) in water. Factors relating to the accident were: an inadquate annual inspection by maintenance personnel, and an inadequate preflight inspection by the pilot.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA96LA187
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB MIA96LA187

Location

Revision history:

Date/timeContributorUpdates
13-Mar-2024 13:26 ASN Update Bot Added

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