ASN Wikibase Occurrence # 357362
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Date: | Wednesday 22 May 1996 |
Time: | 12:45 LT |
Type: | Cessna 310C |
Owner/operator: | Private |
Registration: | N1813H |
MSN: | 35913 |
Total airframe hrs: | 7365 hours |
Engine model: | Continental IO-470-D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Los Lunas, NM -
United States of America
|
Phase: | Landing |
Nature: | Executive |
Departure airport: | Banning, CA (KBNG) |
Destination airport: | Belen, NM (E80) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, the airplane was fully serviced with fuel (130 gal usable) before takeoff. The pilot planned on a fuel consumption of 25 gph per the manufacturer's data, which would have provided a 1 hour fuel reserve. En route the flight encountered forecasted turbulence. The pilot stated that during descent, both engines 'stopped like fuel starvation.' The airplane was maneuvered for a forced landing on a highway, but due to traffic, a railroad right-of-way was selected. During a wheels-up landing, the right wingtip collided with a boulder. The right wing auxillary fuel tank was compromised, and the fuel line separated from the right tip (main) tank, but there was no physical evidence of fuel at the site. About 1 pint of fuel remained in the right main tank; the left main tank was empty. Both fuel selectors were set for the main tanks. During test runs, the left engine rotated, but was not run due to a fuel leak ('O' ring) at the throttle body. The right engine would only run when an external fuel boost pump was 'ON.' An 'O' ring fuel leak was observed at the engine fuel pump, and the pump exhibited a fuel stain from seepage. The fuel pump and the metering unit (after replacing the 'O' ring) flowed within specifications. Both units appeared to be leaking; they were deteriorated and in need of overhaul to change the rubber components. Time since the last annual inspection was 21 hours.
Probable Cause: loss of total engine power due to fuel exhaustion for undetermined reason(s). The lack of suitable terrain for the forced landing was a related factor. The worn and leaking fuel system components and inadequate maintenance by unknown personnel were possible factors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96LA224 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW96LA224
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 17:02 |
ASN Update Bot |
Added |
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