ASN Wikibase Occurrence # 357383
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 18 May 1996 |
Time: | 16:30 LT |
Type: | Maule MX-7-160 |
Owner/operator: | Private |
Registration: | N35TX |
MSN: | 19020C |
Year of manufacture: | 1994 |
Total airframe hrs: | 659 hours |
Engine model: | Lycoming O-320-B2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Belcher, LA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Garland, AR |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was landing at a private airfield on a runway facing the east. The pilot reported he flew the airplane in a 'right hand traffic pattern in order to watch the two windsocks south of the runway and to make sure the tractor that was mowing nearby would remain clear of the runway.' The airplane was on final, with a right cross wind, when the following sequence of events occurred. The pilot stated, 'the aircraft drifted to the north, but I corrected it back, when suddenly a strong gust blew the plane north of the runway. The right wing dropped quickly while we continued to drift left as I added power to execute another go around. The plane continued to drop right wing low, despite my efforts to avoid hitting the ground. The engine accelerated normally, but we struck the ground off to the left of the runway, right wing low.' The airplane came to rest on a heading of approximately 260 degrees on the north side of the runway.
Probable Cause: The pilot's failure to maintain aircraft control in flight. A factor was the gusty wind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96LA218 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW96LA218
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 17:20 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation