Accident Cessna 310R N5079J,
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ASN Wikibase Occurrence # 357824
 
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Date:Wednesday 24 January 1996
Time:13:19 LT
Type:Silhouette image of generic C310 model; specific model in this crash may look slightly different    
Cessna 310R
Owner/operator:Cordair Inc.
Registration: N5079J
MSN: 310R0199
Total airframe hrs:1446 hours
Engine model:Continental TSIO-520
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Fort Pierce, FL -   United States of America
Phase: Approach
Nature:Private
Departure airport:North Eleutria, OF
Destination airport:(KFPR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight was on left base for landing when the left engine lost power. The pilot believed that the right engine would not produce full power. He attempted to land on a road, but the airplane struck a tree and subsequently burned. According to the pilot, when he departed the Bahamas, there was '20 gallons in each main [tank], 30 [gallons] in each auxiliary tank, 20 [gallons] in left wing locker...[the] duration of the flight 1 40, fuel consumption 31 gallons per hour,' or an approximate burn of 52 gallons of fuel. While cruising at 6500 feet, he 'switched' to the auxiliary tanks, 'drained the left wing locker tank' and switched back to the main tanks. Examination of the wreckage revealed the left engine propeller had not been feathered. Also, the landing gear was found extended, and the left engine cowling was intact. The right engine and the right side of the airplane had been consumed by fire damage, but the left engine did not display any fire damage. Both fuel selectors were found positioned to the main fuel tanks. The left engine was placed on a test stand, and a test run was conducted, but no discrepancies were found.

Probable Cause: failure of the pilot to follow emergency procedure(s) and/or feather the respective propeller after loss of power in the left engine for an undetermined reason. The undetermined loss of power (left engine) was a related factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA96LA071
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB MIA96LA071

Revision history:

Date/timeContributorUpdates
14-Mar-2024 06:59 ASN Update Bot Added

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