ASN Wikibase Occurrence # 357969
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Date: | Wednesday 29 November 1995 |
Time: | 14:15 LT |
Type: | Boeing-Stearman B75-N1 |
Owner/operator: | Michael Walsh |
Registration: | N5114N |
MSN: | 75-7721 |
Year of manufacture: | 1943 |
Total airframe hrs: | 11792 hours |
Engine model: | Continental W670-6N |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chino, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | (KCNO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had been asked by a film crew to execute a low pass over the runway. The local controller granted the pilot's request to execute a low pass offset to the north of the runway. When on final approach, the pilot allowed the airspeed to decrease and made a steep approach to the runway. The pilot failed to see the light poles north of the runway. The airplane's left wing contacted the light poles. The pilot did not lose control of the airplane and reentered the traffic pattern landing without further incident.
Probable Cause: the pilot's failure to see and avoid light poles. A poorly planned approach was a factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX96LA066 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX96LA066
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 08:34 |
ASN Update Bot |
Added |
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