ASN Wikibase Occurrence # 358053
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Date: | Sunday 5 November 1995 |
Time: | 15:10 LT |
Type: | Beechcraft K35 Bonanza |
Owner/operator: | Miller Aircraft, Inc. |
Registration: | N5376E |
MSN: | D-5904 |
Total airframe hrs: | 3573 hours |
Engine model: | CONTINENTAL IO-470-C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Phillipsburg, OH -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | (3I7) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHTCREW REPORTED THAT THE COMMERCIAL PILOT/PROSPECTIVE AIRPLANE BUYER, WHO OCCUPIED THE LEFT SEAT, WAS HANDLING THE FLIGHT CONTROLS THROUGHOUT THE LOCAL FLIGHT. THE PILOT IN THE RIGHT SEAT WAS A FLIGHT INSTRUCTOR (CFI). WHEN THE AIRPLANE WAS ON SHORT FINAL APPROACH FOR THE RUNWAY, THE COMMERCIAL PILOT ANNOUNCED THAT HE INTENDED TO EXECUTE A GO-AROUND. BOTH PILOTS REPORTED THAT WHEN THE COMMERCIAL PILOT INITIATED THE GO-AROUND, HE INADVERTENTLY PLACED THE AIRPLANE IN A STEEP NOSE DOWN ATTITUDE. THE CFI STATED THAT HE REACHED FOR THE FLIGHT CONTROL YOKE, AND ATTEMPTED TO PULL THE NOSE UP, BUT THERE WAS NOT ENOUGH ALTITUDE TO RECOVER. THE PILOTS ESTIMATED THAT THE AIRPLANE IMPACTED THE GROUND AT ABOUT A 30 DEGREE NOSE DOWN ATTITUDE. THE AIRPLANE WAS CONFIGURED WITH A SINGLE, THROW OVER YOKE, WHICH WAS POSITIONED TO THE LEFT SIDE OF THE COCKPIT. THE COMMERCIAL PILOT WAS AN EX-MILITARY PILOT WITH VERY LITTLE TIME IN LIGHT PISTON ENGINE AIRPLANES.
Probable Cause: The flight instructor's (CFI's) inadequate supervision of the flying pilot, and the flying pilot's abrupt handling of the airplane during an attempted go-around. Factors relating to the accident were: the flying pilot's lack of familiarity with light piston engine airplanes (kind of aircraft), and the CFI's decision to allow an unfamiliar pilot to attempt the landing, when he (the CFI) did not have access to a full set of flight controls.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | BFO96LA018 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB BFO96LA018
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 09:26 |
ASN Update Bot |
Added |
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