ASN Wikibase Occurrence # 358058
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Date: | Friday 3 November 1995 |
Time: | 21:30 LT |
Type: | Piper PA-28-180 |
Owner/operator: | Charley Wilkerson |
Registration: | N9504J |
MSN: | 28-3625 |
Year of manufacture: | 1966 |
Total airframe hrs: | 5049 hours |
Engine model: | LYCOMING O-360-A3A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Worth, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KFTW) |
Destination airport: | (KFTW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER TAKE OFF AT NIGHT, WHILE CLIMBING THROUGH ABOUT 300 FEET ABOVE GROUND LEVEL, THE ENGINE LOST POWER, AND THE PILOT WAS FORCED TO LAND IN A GRASSY AREA ON AIRPORT PROPERTY. THE LANDING WAS HARD, WHICH RESULTED IN A DAMAGED WING SPAR. THE AIRPLANE HAD BEEN FLOWN APPROXIMATELY 2 HOURS SINCE IT WAS LAST REFUELED. THE PILOT REPORTED THAT HE HAD UTILIZED THE LEFT FUEL TANK FOR THE 2 HOURS OF FLIGHT, AND 'FORGOT TO CHANGE THE FUEL SELECTOR OVER TO THE RIGHT TANK.' ACCORDING TO THE OWNER, EACH FUEL TANK HAD A CAPACITY OF 18 GALLONS, AND FUEL CONSUMPTION WAS APPROXIMATELY 9 GALLONS PER HOUR. EXAMINATION OF THE AIRPLANE AFTER THE ACCIDENT REVEALED THAT THE LEFT MAIN FUEL TANK WAS EMPTY AND THE RIGHT MAIN FUEL TANK WAS FULL. ADDITIONALLY, NO FUEL WAS FOUND IN THE CARBURETOR OR GASCOLATOR. ACCORDING TO THE OWNER'S RECORDS, THE HOBBS METER READING WAS 1345.2 HOURS PRIOR TO THE FLIGHT. THE HOBBS METER READING WAS 1347.2 HOURS AT THE ACCIDENT SITE.
Probable Cause: INADEQUATE PREFLIGHT BY THE PILOT, AND IMPROPER POSITIONING OF THE FUEL SELECTOR, WHICH RESULTED IN FUEL STARVATION AND LOSS OF ENGINE POWER DURING TAKEOFF. DARKNESS WAS A RELATED FACTOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96LA040 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB FTW96LA040
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 09:31 |
ASN Update Bot |
Added |
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