ASN Wikibase Occurrence # 358500
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 8 August 1995 |
Time: | 20:07 LT |
Type: | Mooney M20C |
Owner/operator: | Bms Aviation, Inc. |
Registration: | N9216V |
MSN: | 690050 |
Year of manufacture: | 1969 |
Total airframe hrs: | 1500 hours |
Engine model: | LYCOMING O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Montgomery, PA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Williamsport, PA (IPT |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT AFTER TAKEOFF HE OBSERVED A LOSS OF AIRSPEED, AND THE AIRPLANE WOULD NOT MAINTAIN ALTITUDE. ALSO THE LANDING GEAR FOR UNDETERMINED REASONS WOULD NOT RETRACT. THE PILOT DETERMINED THAT THE ENGINE WAS NOT PRODUCING SUFFICIENT POWER TO SUSTAIN FLIGHT, AND HE INITIATED A FORCED LANDING TO A CORNFIELD. THE ENGINE WAS REMOVED FROM THE AIRPLANE AND TESTED BY AN FAA INSPECTOR, WHO REPORTED, '...NO DISCREPANCIES WERE NOTED DURING THE ENGINE OPERATION TESTING. BOTH MAGNETOS TESTED WITHIN LIMITS. ENGINE PERFORMANCE TESTING REVEALED SLIGHTLY RICH CARBURETOR OPERATION....' THE CARBURETOR WAS TESTED AND AN NTSB INVESTIGATOR REPORTED '...FLOW RATES FOR THE SUBJECT ACCIDENT CARBURETOR WERE SLIGHTLY OUT OF TOLERANCE (EXCESS FLOW) FOR ALL THROTTLE SETTINGS GREATER THAN IDLE. THE GREATEST OUT-OF-TOLERANCE SITUATION OCCURRED AT 3/4 THROTTLE SETTING....'
Probable Cause: The partial loss of engine power, as a result of an excessively rich fuel flow in the carburetor, and a subsequent forced landing. A factor relating to the accident was the malfunction of the landing gear.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC95LA184 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB NYC95LA184
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 15:01 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation