ASN Wikibase Occurrence # 358517
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Date: | Sunday 6 August 1995 |
Time: | 11:50 LT |
Type: | Piper PA-31 |
Owner/operator: | H & H Aviation, Inc. |
Registration: | N9111Y |
MSN: | 31-148 |
Total airframe hrs: | 8460 hours |
Engine model: | LYCOMING TIO-540-A2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Boise, ID -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | , ID (KBOI) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After flying the airplane earlier in the day, the pilot-in-command (Chief Pilot} requested that the engines receive an adjustment for improved performance. The Director of Maintenance performed the adjustments by adjusting the fuel mixture control units on both engines. After the adjustment, the PIC and dual student departed for a Part 135 training flight. No problems were noted during the preflight inspection, engine start-up, taxi, engine run-up, and initial takeoff roll. During climbout, the airplane was unable to climb. The PIC stated that the right engine had a power problem due to the low manifold pressure and he feathered the right propeller to arrest the airplane's descent rate. The airplane continued to descend, and the dual student made the forced landing on rough terrain. Examination of the spark plugs revealed that the engines were operating with an excessively rich mixture. The density altitude was 5,560 feet. This was the dual student's first flight in a Piper PA-31.
Probable Cause: improper adjustment of the engine fuel control units by company maintenance personnel which led to excessive fuel flow and subsequent partial loss of engine power. Factors contributing to the accident were the rough terrain and high density altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA95LA177 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB SEA95LA177
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 15:14 |
ASN Update Bot |
Added |
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