Accident Denney Kitfox 4-1200 (Classic IV) N38HM,
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ASN Wikibase Occurrence # 358518
 
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Date:Sunday 6 August 1995
Time:11:30 LT
Type:Silhouette image of generic FOX model; specific model in this crash may look slightly different    
Denney Kitfox 4-1200 (Classic IV)
Owner/operator:Private
Registration: N38HM
MSN: 1882
Year of manufacture:1995
Total airframe hrs:5 hours
Engine model:ROTAX 912UL
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Weed, CA -   United States of America
Phase: Landing
Nature:Training
Departure airport:(1O6)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE AIRCRAFT OWNER/BUILDER HAD NOT FLOWN SINCE 1988, PENDING RESOLUTION OF A MEDICAL CERTIFICATION PROBLEM. THE PILOT'S MEDICAL WAS RECENTLY REINSTATED AND HE WAS OBTAINING DUAL INSTRUCTION TO COMPLETE A BIENNIAL FLIGHT REVIEW. THE PILOT REPORTED THAT THIS WAS THE SECOND INSTRUCTIONAL FLIGHT OF THE MORNING WITH HIS FLIGHT INSTRUCTOR, AND HAD COMPLETED SIX FULL STOP LANDINGS. DURING THE LAST APPROACH, THE AIRCRAFT DEVELOPED A HIGH SINK RATE ON SHORT FINAL AND THE PILOT SAID HE ADDED A LITTLE POWER, WHICH DID NOT ARREST THE SINK. THE PILOT THEN ADDED FULL POWER. THE HIGH SINK RATE WAS NOT CORRECTED AND THE AIRCRAFT LANDED HARD ON THE RUNWAY, COLLAPSING THE LEFT MAIN LANDING GEAR. THE AIRCRAFT THEN GROUND LOOPED OFF THE RUNWAY.

Probable Cause: the pilot's delayed application of sufficient power to arrest a high sink rate, which resulted in a hard landing. Factors in the accident were the pilot's lack of recent flight experience and the flight instructor's inadequate supervision of the flight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX95LA279
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB LAX95LA279

Location

Revision history:

Date/timeContributorUpdates
14-Mar-2024 15:14 ASN Update Bot Added

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