ASN Wikibase Occurrence # 358565
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Date: | Friday 28 July 1995 |
Time: | 21:00 LT |
Type: | Cessna 402B |
Owner/operator: | Aeroflight Executive Ser. |
Registration: | N51816 |
MSN: | 402B0816 |
Year of manufacture: | 1974 |
Total airframe hrs: | 7162 hours |
Engine model: | CONTINENTAL IO-520-E |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wenatchee, WA -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | (KEAT) |
Destination airport: | Seattle, WA (KBFI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ELEVATOR TRIM JAMMED SHORTLY AFTER TAKEOFF. THE PILOT RETURNED TO THE DEPARTURE AIRPORT, WHILE HOLDING ABOUT 150 POUNDS OF BACK PRESSURE ON THE CONTROL WHEEL. WHEN HE MOVED ONE HAND TO THE THROTTLES TO REDUCE THE POWER, HE WAS UNABLE TO HOLD THE NOSE UP, AND THE AIRCRAFT IMPACTED TERRAIN ABOUT 300 FEET SHORT OF THE APPROACH END OF THE RUNWAY. INVESTIGATION REVEALED THAT COMPANY MAINTENANCE PERSONNEL HAD FAILED TO INSTALL A COTTER KEY, AND THE TRIM TAB PUSH ROD ATTACHMENT BOLT, NUT, AND COTTER KEY WERE MISSING.
Probable Cause: IMPROPER INSTALLATION (FAILURE TO INSTALL COTTER KEY) BY COMPANY MAINTENANCE PERSONNEL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA95LA159 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB SEA95LA159
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 15:46 |
ASN Update Bot |
Added |
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