ASN Wikibase Occurrence # 358605
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Date: | Sunday 23 July 1995 |
Time: | 10:00 LT |
Type: | Bellanca 17-31ATC |
Owner/operator: | Private |
Registration: | N500BT |
MSN: | 74-31104 |
Total airframe hrs: | 1154 hours |
Engine model: | LYCOMING IO-540-K |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hico, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Conroe, TX (KCXO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHEN THE PILOT APPLIED POWER 'RAPIDLY' TO GO AROUND AFTER A 'LONG' TOUCHDOWN ON THE 2,300 FOOT GRASS STRIP, THE ENGINE 'HESITATED'. AFTER BECOMING AIRBORNE, THE PILOT TURNED LEFT TO AVOID HITTING TREES AT THE END OF THE RUNWAY. THE AIRPLANE THEN STRUCK A FENCE AND IMPACTED THE GROUND. EXAMINATION OF THE PROPELLER BY AN FAA INSPECTOR REVEALED SIGNATURES INDICATING THE ENGINE WAS OPERATING AT A HIGH POWER SETTING DURING IMPACT.
Probable Cause: THE PILOT'S FAILURE TO ATTAIN THE PROPER TOUCHDOWN POINT AND THE DELAYED GO-AROUND.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW95LA311 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW95LA311
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 16:13 |
ASN Update Bot |
Added |
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