ASN Wikibase Occurrence # 358833
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 20 June 1995 |
Time: | 15:09 LT |
Type: | Ed Bergreen KIS |
Owner/operator: | Private |
Registration: | N62TW |
MSN: | 025 |
Total airframe hrs: | 37 hours |
Engine model: | LYCOMING O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Leandro, CA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | San Jose, CA (KSJC) |
Destination airport: | Santa Rosa, CA (KSTS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID THE AIRPLANE CONTAINED 17 GALLONS OF FUEL IN THE WING TANKS BEFORE DEPARTING ON THE ACCIDENT FLIGHT. ABOUT 5 MINUTES INTO THE FLIGHT, THE ENGINE BEGAN TO SPUTTER. HE ADVISED ATC THAT THE ENGINE WAS MISSING AND RECEIVED RADAR VECTORS TOWARD THE NEAREST AIRPORT. THE PILOT OVERFLEW THE NEAREST AIRPORT TO LAND AT ANOTHER AIRPORT, THINKING THAT THE AIRPLANE ALTITUDE WAS SUFFICIENT TO NEGOTIATE THE SELECTED AIRPORT IF THERE WAS A TOTAL LOSS OF POWER. THE ENGINE QUIT WHILE ON FINAL APPROACH TO THE SELECTED AIRPORT AND THE PILOT WAS UNABLE TO MAKE THE RUNWAY AND LANDED BEHIND A MIDDLE SCHOOL. EXAMINATION OF THE WRECKAGE REVEALED THAT NEITHER THE AIRFRAME NOR ENGINE FUEL SYSTEMS WERE COMPROMISED AND THAT THE LEFT WING FUEL TANK CONTAINED ONLY RESIDUAL FUEL AND THE RIGHT WING FUEL TANK WAS EMPTY. INVESTIGATORS WERE UNABLE TO DRAIN ANY FUEL FROM THE GASCOLATOR.
Probable Cause: the pilot's poor preflight preparation and in-flight decision to overfly a suitable airport when it was evident that he was having an engine problem. The fuel exhaustion was a factor in this accident.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX95LA218 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB LAX95LA218
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 18:41 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation