Accident Aerospatiale AS-350B N35AH,
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ASN Wikibase Occurrence # 358989
 
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Date:Friday 19 May 1995
Time:20:10 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Aerospatiale AS-350B
Owner/operator:American Helicopter Special.
Registration: N35AH
MSN: 2244
Year of manufacture:1989
Total airframe hrs:1782 hours
Engine model:TURBOMECA ARRIEL I B
Fatalities:Fatalities: 0 / Occupants: 6
Aircraft damage: Substantial
Category:Accident
Location:Tampa, FL -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:(KTPF)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT STATED HE FELT A FEEDBACK IN THE CYCLIC CONTROL AND THE CONTROLS LOCKED AS HE MADE A SHALLOW LEFT TURN AT ABOUT 800 FEET. THE HELICOPTER ENTERED A DESCENDING LEFT TURN TOWARD AN ISLAND AND THE PILOT RECEIVED INTERMITTENT HYDRAULIC SYSTEM FAILURE INDICATIONS BUT DID NOT FOLLOW MANUFACTURER'S PROCEDURES FOR HYDRAULIC SYSTEM FAILURE WHICH CALL FOR REDUCTION OF AIRSPEED TO BETWEEN 40 AND 60 KNOTS AND TURNING OFF OF THE HYDRAULIC SYSTEM. HE WAS UNABLE TO REGAIN CONTROL OF THE HELICOPTER PRIOR TO TOUCHING DOWN HARD, TAIL FIRST ON THE ISLAND. THE HELICOPTER THEN SKIDDED INTO THE WATER AND CAME TO REST. POST CRASH EXAMINATION SHOWED THE HYDRAULIC MANIFOLD AND FILTER WERE CLOGGED WITH DEBRIS FROM THE CORROSION OF THE MANIFOLD AND FILTER CAP. MANUFACTURER'S PROCEDURES REQUIRE THE FILTER AND MANIFOLD TO BE EXAMINED AT EACH 500 HOUR INSPECTION. THE HELICOPTER HAD RECEIVED A 500 HOUR INSPECTION ABOUT 6 WEEKS AND 50 FLIGHT HOURS BEFORE THE ACCIDENT.

Probable Cause: THE FAILURE OF THE PILOT TO FOLLOW MANUFACTURERS PROCEDURES AFTER FAILURE OF THE HYDRAULIC SYSTEM RESULTING IN LOSS OF CONTROL OF THE HELICOPTER. CONTRIBUTING TO THE ACCIDENT WAS THE FAILURE OF MAINTENANCE PERSONNEL TO FOLLOW MANUFACTURERS PROCEDURES FOR MAINTENANCE OF THE HYDRAULIC SYSTEM.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA95LA131
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB MIA95LA131

Revision history:

Date/timeContributorUpdates
14-Mar-2024 20:23 ASN Update Bot Added

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