ASN Wikibase Occurrence # 35929
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Date: | Monday 7 September 1992 |
Time: | 13:40 LT |
Type: | Beechcraft C-45G Expeditor |
Owner/operator: | Exa, Incorporated |
Registration: | N3657G |
MSN: | AF461 |
Year of manufacture: | 1951 |
Total airframe hrs: | 7780 hours |
Engine model: | P&W R-985-AN-14B |
Fatalities: | Fatalities: 12 / Occupants: 12 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hinckley, IL -
United States of America
|
Phase: | Initial climb |
Nature: | Parachuting |
Departure airport: | (OC2) |
Destination airport: | (OC2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER TAKEOFF, THE AIRPLANE WAS SEEN AT LOW ALTITUDE TRAILING SMOKE FROM THE LEFT ENGINE. WITNESSES SAW THE WINGS 'TIPPING' BACK AND FORTH, THEN A WING DROPPED AND HIT THE GROUND. EXAMINATION REVEALED THAT A SUPERCHARGER BEARING HAD FAILED IN THE LEFT ENGINE. THE LEFT ENGINE HAD BEEN RECENTLY INSTALLED BY NON-CERTIFICATED PERSONNEL AFTER BEING INACTIVE FOR 18 YRS WITHOUT PRESERVATION. THE AIRPLANE HAD FLOWN ABOUT 184 HRS SINCE THE LAST ANNUAL INSPECTION; NO RECORD OF SUBSEQUENT 100-HR INSPECTION. THE LEFT PROP BLADES WERE FOUND IN AN INTERMEDIATE POSITION BETWEEN THE OPERATING RANGE AND THE FEATHERED POSITION. THE LEFT PROP WAS CHANGED SEVERAL WEEKS PRIOR TO THE ACCIDENT. THERE IS NO EVIDENCE THAT THE LEFT PROP HAD EVER BEEN SUCCESSFULLY CYCLED TO THE FULL FEATHER POSITION. THE OPERATOR AND PILOTS WERE NOT AWARE OF HAMILTON STANDARD SB 657 RECOMMENDING FULL-FEATHER CHECKS EVERY 30 DAYS. LEFT PROP FEATHERING MOTOR RELAYS NOT RECOVERED. ALL 11 PARACHUTISTS WERE FOUND IN CENTER PART OF FUSELAGE; NO EVIDENCE OF RESTRAINT USEAGE.
Probable Cause: INADEQUATE MAINTENANCE AND INSPECTION BY THE OPERATOR WHICH RESULTED IN AN ENGINE POWER LOSS DURING THE CRITICAL TAKEOFF PHASE OF FLIGHT. IN ADDITION, THE PILOT DID NOT, OR WAS UNABLE TO, ATTAIN A FULL-FEATHER POSITION ON THE LEFT ENGINE PROPELLER, WHICH WOULD HAVE MOST LIKELY ENABLED THE AIRPLANE TO SUSTAIN MINIMUM CONTROL AIRSPEED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DCA92MA048 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB DCA92MA048
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
08-Apr-2011 15:02 |
TB |
Updated [Time, Aircraft type, Cn, Operator, Phase, Nature, Source] |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 18:07 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
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