ASN Wikibase Occurrence # 359344
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Date: | Monday 13 February 1995 |
Time: | 14:40 LT |
Type: | Taylorcraft F19 |
Owner/operator: | Private |
Registration: | N20001 |
MSN: | 126 |
Total airframe hrs: | 806 hours |
Engine model: | CONTINENTAL O-200 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tullahoma, TN -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Tullamoma, TN (THA |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT ABOUT 20 MINUTES AFTER TAKEOFF, WHILE MANEUVERING NEAR HIS RESIDENCE, THE AIRCRAFT ENGINE LOST POWER. HE MADE AN EMERGENCY LANDING IN A FIELD, BUT THE AIRPLANE HIT A FENCE AND ENCOUNTERED UNEVEN TERRAIN DURING THE LANDING. EXAMINATION OF THE ENGINE REVEALED THAT THE STARTER ROLLER CLUTCH, WHICH HAD BEEN INSTALLED IN THE AIRCRAFT IMMEDIATELY BEFORE THE FLIGHT, HAD SEIZED. THE ROLLER CLUTCH WAS IN PLACE, BUT THE ROLLERS WERE FOUND TO HAVE MELTED AND HAD WELDED TO THE SHAFT. SUBSEQUENTLY, ALL FOUR OF THE CRANKSHAFT GEAR CAPSCREWS HAD FAILED, RESULTING IN DISENGAGEMENT OF THE CRANKSHAFT GEAR AND SUBSEQUENT POWER LOSS. A SERVICE BULLETIN (TELEDYNE CONTINENTAL M79-10) HAD BEEN ISSUED BY THE MANUFACTURER IN JUNE OF 1979 TO PROVIDE PRESSURIZED LUBRICATION OF THE ROLLER CLUTCH STARTERS, BUT THE SERVICE BULLETIN HAD NOT BEEN ACCOMPLISHED. THE ENGINE HAD BEEN SHIPPED FROM THE FACTORY ON 5/26/78 (BEFORE THE SERVICE BULLETIN WAS ISSUED). THE STARTER INSTALLATION INSTRUCTIONS DID NOT REQUIRE THAT THE SERVICE BULLETIN BE COMPLIED WITH BEFORE INSTALLATION OF THE STARTER. THERE WAS EVIDENCE THAT THE STARTER ROLLER CLUTCH LACKED ADEQUATE LUBRICATION.
Probable Cause: A LACK OF LUBRICANT TO THE STARTER/ROLLER CLUTCH, SEIZURE OF THE STARTER, AND FAILURE OF THE FOUR CRANKSHAFT GEAR CAPSCREWS (BOLTS), WHICH RESULTED IN DISENGAGEMENT OF THE CRANKSHAFT (ACCESSORY) GEAR AND SUBSEQUENT LOSS OF ENGINE POWER.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL95LA051 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB ATL95LA051
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 09:33 |
ASN Update Bot |
Added |
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