ASN Wikibase Occurrence # 359353
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 7 February 1995 |
Time: | 16:23 LT |
Type: | Cessna 152 |
Owner/operator: | Mc Aviation, Inc. |
Registration: | N757XX |
MSN: | 15280096 |
Total airframe hrs: | 5302 hours |
Engine model: | LYCOMING O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mobile, AL -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AS THE PILOT WAS RETURNING TO THE AIRPORT, HE TRANSMITTED THAT THE ENGINE HAD LOST POWER. AT THAT TIME, HE WAS TOO FAR AWAY TO REACH THE AIRPORT AND STATED THAT HE WOULD HAVE TO LAND 'JUST BELOW.' A WITNESS HEARD THE POWER INTERRUPTIONS AND SAW THE AIRPLANE CIRCLE AN AREA WITH A DIRT PIT, LANDFILL, AND ROADWAY. A WITNESS IN A VEHICLE ON THE ROADWAY OBSERVED THE AIRPLANE AT LOW ALTITUDE (ESTIMATED 75 TO 100 FEET AGL). HE OBSERVED THAT THE AIRPLANE THEN DESCENDED IN A NOSE AND RIGHT WING LOW ATTITUDE, BEFORE IT CRASHED. WHEN HE ARRIVED AT THE CRASH SITE, HE NOTED OIL DRAINING FROM THE AIRPLANE, BUT DID NOT SEE ANY FUEL LEAKAGE, THOUGH NUMEROUS FUEL LINES WERE SEVERED. NO PREIMPACT MECHANICAL FAILURE WAS NOTED DURING THE INVESTIGATION. THE FUEL SELECTOR WAS FOUND IN THE 'OFF' POSITION AND 1.3 GAL OF FUEL WAS DRAINED FROM THE FUEL TANKS. ACCORDING TO THE PILOT'S OPERATING HANDBOOK, 1.5 GAL OF THE FUEL SUPPLY WAS UNUSABLE. RECORDS SHOWED THAT THE AIRPLANE HAD BEEN FLOWN 3.5 HOURS SINCE IT WAS LAST REFUELED.
Probable Cause: THE PILOT'S IMPROPER PLANNING/DECISION, WHICH RESULTED IN FUEL EXHAUSTION BEFORE REACHING THE AIRPORT, AND HIS FAILURE TO MAINTAIN ADEQUATE AIRSPEED WHILE MANEUVERING FOR A FORCED LANDING, WHICH RESULTED IN AN INADVERTENT STALL AND COLLISION WITH THE TERRAIN.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA95FA072 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB MIA95FA072
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 09:40 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation