ASN Wikibase Occurrence # 359599
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Date: | Wednesday 2 November 1994 |
Time: | 11:20 LT |
Type: | Boeing 747-251B |
Owner/operator: | Northwest Airlines |
Registration: | N631US |
MSN: | 23111/594 |
Year of manufacture: | 1984 |
Total airframe hrs: | 40562 hours |
Engine model: | P&W JT9D-7R4 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Chicag0, IL -
United States of America
|
Phase: | Taxi |
Nature: | Ferry/positioning |
Departure airport: | Detroit, MI (KDTW) |
Destination airport: | Chicago, IL (KORD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLT CREW DISCONNECTED THE NUMBER ONE ENG CONSTANT SPEED DRIVE (CSD) DURING A FLT ON THE DAY PRIOR TO THIS INCIDENT WHEN ITS OIL PRESSURE LIGHT ILLUMINATED. DUE TO OTHER, UNRELATED MAINTENANCE, THE AIRPLANE'S NEXT REVENUE FLT WAS CANCELLED. SECOND SHIFT MECHANICS WERE ASSIGNED MAINTENANCE ON THE AIRPLANE. THE MECHANICS DECIDED TO TROUBLESHOOT THE UNIT. THE CSD WAS MECHANICALLY RECOUPLED AND THE ENG WAS STARTED. AFTER THE ENG START, THE START VALVE LIGHT FAILED TO GO OUT AND THE ENGINE WAS SHUT DOWN. A MECHANIC REMOVED THE MAIN CSD WIRING HARNESS CANNON PLUG TO HELP WITH THE TROUBLE SHOOTING PROCESS. THE START VALVE WAS REPLACED AND THE ENG WAS RUNUP. THE CSD CANNON PLUG WAS NOT CONNECTED AT THE CONCLUSION OF THE ENG RUNUP. AFTER SHUTDOWN THE START VALVE CHANGE WAS ENTERED INTO THE AIRPLANE MAINTENANCE RECORDS. THE MECHANIC WHO RECOUPLED THE CSD INFORMED THE LEAD MECHANIC OF HIS ACTION BEFORE HE LEFT FOR THE DAY. ACCORDING TO THE COMPANY, THE THIRD SHIFT MECHANICS DID NOT HAVE ENOUGH TIME TO CHANGE THE CSD. THE NUMBER ONE ENG WAS '...CLOSED UP [AND] THE AIRCRAFT WAS DISPATCHED.' DURING TAXI FROM LANDING THE CSD CAUGHT FIRE.
Probable Cause: inattentive maintenance service of the airplane by the mechanic who failed to disengage the constant speed drive (CSD) after the engine runup had been completed. A factor in this incident was the lead mechanic not performing maintenance record keeping after being informed that the CSD had been recoupled.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI95IA028 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB CHI95IA028
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 12:38 |
ASN Update Bot |
Added |
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