Serious incident Boeing 747-251B N631US,
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ASN Wikibase Occurrence # 359599
 
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Date:Wednesday 2 November 1994
Time:11:20 LT
Type:Silhouette image of generic B742 model; specific model in this crash may look slightly different    
Boeing 747-251B
Owner/operator:Northwest Airlines
Registration: N631US
MSN: 23111/594
Year of manufacture:1984
Total airframe hrs:40562 hours
Engine model:P&W JT9D-7R4
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Minor
Category:Serious incident
Location:Chicag0, IL -   United States of America
Phase: Taxi
Nature:Ferry/positioning
Departure airport:Detroit, MI (KDTW)
Destination airport:Chicago, IL (KORD)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE FLT CREW DISCONNECTED THE NUMBER ONE ENG CONSTANT SPEED DRIVE (CSD) DURING A FLT ON THE DAY PRIOR TO THIS INCIDENT WHEN ITS OIL PRESSURE LIGHT ILLUMINATED. DUE TO OTHER, UNRELATED MAINTENANCE, THE AIRPLANE'S NEXT REVENUE FLT WAS CANCELLED. SECOND SHIFT MECHANICS WERE ASSIGNED MAINTENANCE ON THE AIRPLANE. THE MECHANICS DECIDED TO TROUBLESHOOT THE UNIT. THE CSD WAS MECHANICALLY RECOUPLED AND THE ENG WAS STARTED. AFTER THE ENG START, THE START VALVE LIGHT FAILED TO GO OUT AND THE ENGINE WAS SHUT DOWN. A MECHANIC REMOVED THE MAIN CSD WIRING HARNESS CANNON PLUG TO HELP WITH THE TROUBLE SHOOTING PROCESS. THE START VALVE WAS REPLACED AND THE ENG WAS RUNUP. THE CSD CANNON PLUG WAS NOT CONNECTED AT THE CONCLUSION OF THE ENG RUNUP. AFTER SHUTDOWN THE START VALVE CHANGE WAS ENTERED INTO THE AIRPLANE MAINTENANCE RECORDS. THE MECHANIC WHO RECOUPLED THE CSD INFORMED THE LEAD MECHANIC OF HIS ACTION BEFORE HE LEFT FOR THE DAY. ACCORDING TO THE COMPANY, THE THIRD SHIFT MECHANICS DID NOT HAVE ENOUGH TIME TO CHANGE THE CSD. THE NUMBER ONE ENG WAS '...CLOSED UP [AND] THE AIRCRAFT WAS DISPATCHED.' DURING TAXI FROM LANDING THE CSD CAUGHT FIRE.

Probable Cause: inattentive maintenance service of the airplane by the mechanic who failed to disengage the constant speed drive (CSD) after the engine runup had been completed. A factor in this incident was the lead mechanic not performing maintenance record keeping after being informed that the CSD had been recoupled.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI95IA028
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB CHI95IA028

Revision history:

Date/timeContributorUpdates
15-Mar-2024 12:38 ASN Update Bot Added

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