ASN Wikibase Occurrence # 359673
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 13 October 1994 |
Time: | 16:05 LT |
Type: | Piper PA-24-250 |
Owner/operator: | Private |
Registration: | N6976P |
MSN: | 24-2119 |
Total airframe hrs: | 4220 hours |
Engine model: | LYCOMING O-540-A1A5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lone Pine, CA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | (O26) |
Destination airport: | Chino, CA (KCNO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID HE BEGAN TO EXPERIENCE DIRECTIONAL CONTROL PROBLEMS DURING THE GROUND ROLL. THE AIRPLANE DID NOT SEEM TO RESPOND TO RIGHT RUDDER INPUTS, AND HE LIFTED OFF EARLY TO AVOID DEPARTING THE LEFT SIDE OF THE PAVEMENT. THE AIRCRAFT DID NOT HAVE ADEQUATE AIRSPEED AND SETTLED BACK TO THE GROUND IN A LEFT DRIFT. THE RIGHT MAIN LANDING GEAR COLLAPSED AND THE AIRCRAFT SPUN AROUND TO A STOP. THE MANAGER AT THE AIRPORT EXAMINED THE AIRCRAFT AND REPORTED THAT THE NOSE GEAR APPEARED TO BE INTACT. THE RIGHT LINKAGE WHICH CONNECTS THE NOSE GEAR STEERING COLLAR TO THE RUDDER PEDALS WAS BROKEN, WITH A PIECE MISSING. HE ALSO REPORTED THAT HE INSPECTED THE TAXIWAY AND RUNWAY, BUT DID NOT FIND THE MISSING PIECE. IN HIS REPORT, THE PILOT NOTED THAT THE MISSING PIECE WAS FOUND 50 FT WEST OF THE CRASH SITE. HE STATED THAT THE FRACTURE FACE EXHIBITED A RUST-COLORED APPEARANCE OVER ABOUT 1/2 OF THE FRACTURE, WITH THE REMAINDER SHINY IN APPEARANCE. THE PART WAS NOT PROVIDED TO NTSB FOR EXAMINATION AS REQUESTED.
Probable Cause: THE PILOT'S FAILURE TO ABORT THE TAKEOFF, RESULTING IN A PREMATURE LIFT-OFF. A FACTOR IN THE ACCIDENT WAS THE FAILURE OF THE STEERING LINKAGE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX95LA006 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX95LA006
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 13:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation