ASN Wikibase Occurrence # 360234
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 2 July 1994 |
Time: | 23:37 LT |
Type: | Cessna 150M |
Owner/operator: | Private |
Registration: | N63277 |
MSN: | 15077225 |
Year of manufacture: | 1975 |
Total airframe hrs: | 3757 hours |
Engine model: | CONTINENTAL O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Waseca, MN -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Brookings, SD (KBKX) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT UPON NEARING THE DESTINATION AIRPORT THE ENGINE BEGAN RUNNING ROUGH AND LOST POWER. A FORCED LANDING WAS MADE DURING WHICH THE AIRPLANE CONTACTED A DITCH AND CAME TO REST INVERTED IN A CORN FIELD. POST ACCIDENT INSPECTION REVEALED 45 OUNCES OF FUEL REMAINED ON BOARD THE AIRPLANE. THE PILOT STATED THAT BETTER PREFLIGHT PLANNING COULD HAVE PREVENTED THE ACCIDENT.
Probable Cause: inadequate preflight planning/preparation and the pilot's failure to refuel the airplane. Factors related to the accident were a poorly planned forced landing approach and high vegetation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI94LA219 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB CHI94LA219
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 19:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation