ASN Wikibase Occurrence # 360476
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Date: | Sunday 15 May 1994 |
Time: | 21:00 LT |
Type: | Stinson 108-2 |
Owner/operator: | Private |
Registration: | N9761K |
MSN: | 108-2761 |
Year of manufacture: | 1947 |
Engine model: | FRANKLIN 165-B3 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kettle River, MN -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THE ENGINE LOST RPM, SPUTTERED AND STOPPED ABOUT 10-12 SECONDS AFTER TAKEOFF. THE AIRPLANE STRUCK SOME TREES DURING THE FORCED LANDING. FAA INSPECTORS WHO EXAMINED THE AIRPLANE COULD FIND NO ENGINE ANOMALY WHICH WOULD CAUSE A LOSS OF POWER. THE TEMPERATURE WAS 51 DEGREES, AND THE DEW POINT WAS 43 DEGREES. THESE TEMPERATURE/DEW POINT CONDITIONS ARE FAVORABLE FOR SERIOUS CARBURETOR ICING. THE PILOT STATED HE DID A CARBURETOR HEAT CHECK ON RUN-UP. THE FAA INSPECTOR WHO EXAMINED THE WRECKAGE REPORTED THE CARBURETOR HEAT WAS IN THE 'OFF' POSITION.
Probable Cause: THE PILOT'S IMPROPER USE OF CARBURETOR HEAT AND THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING. THE CARBURETOR ICING WEATHER CONDITION WAS A FACTOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI94LA163 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI94LA163
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 07:43 |
ASN Update Bot |
Added |
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