ASN Wikibase Occurrence # 360782
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Date: | Wednesday 2 March 1994 |
Time: | 15:50 LT |
Type: | Hughes 269C |
Owner/operator: | Private |
Registration: | N9593F |
MSN: | 540307 |
Total airframe hrs: | 3344 hours |
Engine model: | LYCOMING HIO-360-O1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Merced, CA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | |
Destination airport: | Stockton, CA (KSCK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on a flight test for a CFI certificate with an FAA inspector. The inspector directed the pilot/applicant to perform a practice 180-degree autorotation, terminating with a power recovery. Upon entry, at 650 feet agl, the needles split, the rotor rpm was in the green, and the engine stabilized at 2,000 RPM. During the maneuver, the inspector noted that the helicopter was apparently going to overshoot the termination point. About 50 feet agl, the pilot began deceleration and the aircraft began to settle. At that point, the inspector still had not heard the engine rpm increase. Concerned that the throttle had not been rolled on, he took the controls and attempted to open the throttle. In spite of his efforts, the helicopter continued to settle, touched down hard about 100 feet beyond the termination point, bounced once, pitched forward, and then impacted a second time. The helicopter then rolled tail over nose finally coming to rest on its right side. A postaccident inspection failed to identify any discrepancies in the engine or power controls.
Probable Cause: the pilot's misjudgement of the descent rate and his delayed throttle application.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX94LA146 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX94LA146
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 11:05 |
ASN Update Bot |
Added |
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