ASN Wikibase Occurrence # 360960
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 27 December 1993 |
Time: | 20:23 LT |
Type: | Piper PA-28-181 |
Owner/operator: | Private |
Registration: | N4320X |
MSN: | 28-7690003 |
Total airframe hrs: | 2364 hours |
Engine model: | LYCOMING O-360-A4M |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Greer, SC -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Baltimore, MD (KBWI) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT WAS ON APPROACH FOR GREENVILLE SPARTANBURG AIRPORT WHEN THE PILOT ADVISED AIR TRAFFIC CONTROL THAT HE HAD TWENTY MINUTES OF FUEL LEFT. ATC OFFERED VECTORS TO ANOTHER AIRPORT WHICH WAS THREE MILES FROM HIS POSITION, BUT THE PILOT DECLINED. SHORTLY AFTER, THE PILOT REQUESTED A DIVERSION TO THE ALTERNATE AIRPORT , WHICH ATC APPROVED. APPROXIMATELY TWO MILES FROM THE ALTERNATE AIRPORT, THE PILOT REPORTED THAT HE HAD LOST ENGINE POWER AND WOULD HAVE TO PERFORM AN EMERGENCY LANDING. ATC ADVISED THE PILOT OF A HIGHWAY LESS THAN ONE MILE FROM HIS POSITION. DURING THE EMERGENCY APPROACH, THE PILOT ATTEMPTED A 180 DEGREE TURN TO AVOID ONCOMING AUTOMOTIVE TRAFFIC AND THE AIRPLANE IMPACTED TREES OFF OF THE HIGHWAY. THE PILOT REPORTED CALCULATING TWENTY MINUTES OF RESERVE FUEL DURING PREFLIGHT PLANNING. HE STATED THAT DURING THE FLIGHT, HE OBSERVED THAT HIS ACTUAL TIME ENROUTE WAS LESS THAN HE HAD PLANNED, AND THOUGHT HE WOULD HAVE ENOUGH FUEL FOR THE FLIGHT. HE STATED THAT HE FAILED TO TAKE INTO ACCOUNT HIS USE OF 75% POWER DURING THE FLIGHT INSTEAD OF 65% HE HAD USED FOR PREFLIGHT PLANNING, AND THE ADDITIONAL FUEL BURN AS A RESULT.
Probable Cause: THE PILOT'S INADEQUATE IN-FLIGHT PLANNING IN DETERMINING FUEL REQUIREMENTS FOR THE FLIGHT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL94LA034 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB ATL94LA034
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 13:16 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation