Accident Hughes 369D N115HD,
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ASN Wikibase Occurrence # 360972
 
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Date:Wednesday 22 December 1993
Time:10:00 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369D
Owner/operator:Smokey Mountain Helicopters
Registration: N115HD
MSN: 711020D
Year of manufacture:1981
Total airframe hrs:2803 hours
Engine model:Allison 250 C20B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Waimea, Kauai, HI -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Unknown
Departure airport:Hanapepe, HI (PAK)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DURING AN EXTERNAL LOAD OPERATION, THE ENGINE STOPPED PRODUCING POWER. DURING AUTOROTATION INTO A RIVER BED AREA, THE HELICOPTER CONTACTED A BOULDER & ROLLED OVER. ENG EXAM REVEALED A COLLAPSED FUEL INLET SCREEN IN THE FUEL NOZZLE RESTRICTING FUEL FLOW. HEAVY CONTAMINATION, LATER DETERMINED TO BE A SODIUM-RICH SILICON MATERIAL, WAS NOTED ON THE SCREEN. THE HELICOPTER WAS OPERATED EXCLUSIVELY IN A MARINE ENVIRONMENT, AND THE OPERATOR PERFORMED A DAILY COMPRESSOR WASH PROCEDURE IN ACCORDANCE WITH THE ENGINE MANUFACTURER'S SERVICE LETTER. THE SPECIFIED PROCEDURE RESULTED IN IMMERSION OF THE FUEL NOZZLE IN SODIUM-CONTAMINATED WASH WATER, WITH SUBSEQUENT SOLUTION INFILTRATION INTO THE FUEL NOZZLE INLET SCREEN. THE SCREEN HAS A LIFE LIMIT OF 2,500 HRS AND IS NOT SUBJECT TO ANY ROUTINE INSPECTION REQUIREMENTS.

Probable Cause: AN INADEQUATE ENGINE COMPRESSOR CLEANING PROCEDURE SPECIFIED IN THE MANUFACTURER'S SERVICE LETTER, WHICH RESULTED IN THE TOTAL LOSS OF ENGINE POWER DUE TO CONTAMINATION, BLOCKAGE, AND COLLAPSE OF THE FUEL NOZZLE INLET SCREEN. FACTORS IN THE ACCIDENT WERE: THE LACK OF A SPECIFIED PERIODIC INSPECTION REQUIREMENT FOR THE NOZZLE SCREEN AND THE UNSUITABLE NATURE OF THE TERRAIN FOR THE FORCED LANDING.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX94LA076
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB LAX94LA076

Location

Revision history:

Date/timeContributorUpdates
16-Mar-2024 13:23 ASN Update Bot Added

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