Accident Beechcraft 200 Super King Air N191FL,
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ASN Wikibase Occurrence # 361119
 
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Date:Thursday 28 October 1993
Time:00:15 LT
Type:Silhouette image of generic BE20 model; specific model in this crash may look slightly different    
Beechcraft 200 Super King Air
Owner/operator:Private
Registration: N191FL
MSN: BB-107
Total airframe hrs:6420 hours
Engine model:P&W PT6A-42
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:Reno, NV -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(KRNO)
Destination airport:San Carlos, CA (KSQL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
AFTER MOVING THE LANDING GEAR HANDLE TO THE UP POSITION, THE COCKPIT BEGAN FILLING WITH SMOKE. THE PILOT NOTICED THAT THE GEAR APPEARED TO BE HUNG IN AN INTRANSIT POSITION. THE SMOKE, WHICH SMELLED OF BURNING ELECTRICAL INSULATION, BECAME HEAVIER, AND HEAT COULD BE FELT ON THE COCKPIT FLOOR.THE PILOT RETURNED TO THE AIRPORT, AND THE GEAR COLLAPSED DURING LANDING. EXAMINATION REVEALED THAT THE LANDING GEAR MOTOR AND ASSOCIATED WIRING WERE BURNED, AND THE COCKPIT FLOORING APPEARED TO BE PARTIALLY MELTED. THE RIGHT LANDING GEAR ACTUATOR WAS FOUND TO HAVE BEEN IMPROPERLY OVERHAULED, WHICH RESULTED IN THREE GEAR TEETH BREAKING AND JAMMING THE ACTUATOR. BEECH MANDATORY SERVICE BULLETIN NO. 2035, REV. II, REQUIRING REPLACEMENT OF THE 200-AMP GEAR MOTOR CIRCUIT BREAKER WITH A 60-AMP BREAKER TO PREVENT GEAR MOTOR DAMAGE, WAS NOT ACCOMPLISHED ON THIS AIRPLANE.

Probable Cause: THE IMPROPER OVERHAUL OF THE RIGHT MAIN LANDING GEAR ACTUATOR BY MAINTENANCE PERSONNEL, AND THE OPERATOR'S FAILURE TO ASSURE THAT THE AIRPLANE MANUFACTURER'S MANDATORY SERVICE BULLETIN REQUIRING MODIFICATION OF THE GEAR MOTOR CIRCUIT PROTECTION WAS ACCOMPLISHED.

Accident investigation:
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Investigating agency: NTSB
Report number: LAX94LA030
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX94LA030

History of this aircraft

Other occurrences involving this aircraft
27 October 1993 N191FL Edward A. Mueller 0 Reno-Cannon International Airport, NV (RNO) sub

Location

Revision history:

Date/timeContributorUpdates
16-Mar-2024 14:59 ASN Update Bot Added

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