Serious incident Short 360-200 N711HJ,
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ASN Wikibase Occurrence # 361889
 
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Date:Monday 14 June 1993
Time:17:02 LT
Type:Silhouette image of generic SH36 model; specific model in this crash may look slightly different    
Short 360-200
Owner/operator:Pennsylvania Commuter
Registration: N711HJ
MSN: SH3697
Total airframe hrs:15829 hours
Engine model:P&W PT6A-65AR
Fatalities:Fatalities: 0 / Occupants: 21
Aircraft damage: None
Category:Serious incident
Location:Atlantic City, NJ -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Philadelphia, PA (PHL
Destination airport:New Haven, CT (KHVN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE AIRPLANE WAS CRUISING AT 6000 FEET WHEN THE AFT BAGGAGE COMPARTMENT FIRE LIGHT ILLUMINATED IN THE COCKPIT. EXTINGUISHING AGENT WAS DIRECTED TO THE AFT BAGGAGE COMPARTMENT BY THE FLIGHT ATTENDANT PLACING THE NOZZLE OF A HAND HELD FIRE EXTINGUISHER THROUGH A RECEPTACLE WITH A SEALING 'O' RING, LOCATED ON THE AFT CABIN BULKHEAD. THE FLIGHT ATTENDANT SAID THE EXTINGUISHING AGENT BLEW BACK ONTO HER HANDS. SHE THEN TRIED TWO OTHER EXTINGUISHERS WITH THE SAME RESULTS. AFTER LANDING, EXAMINATION OF THE BAGGAGE COMPARTMENT FOUND NO EVIDENCE OF A FIRE. THE FIRE WARNING WAS ATTRIBUTED TO A FALSE INDICATION FROM THE SMOKE DETECTOR IN THE AFT BAGGAGE COMPARTMENT. POST INCIDENT TESTING BY THE FAA AND THE OPERATOR FOUND THAT WHEN THE FIRE EXTINGUISHER NOZZLE DID NOT FIT THORUGH THE SEALING 'O' RING, EXTINGUISHING AGENT WOULD SPRAY BACK ON THE PERSON HOLDING THE FIRE EXTINGUISHER. WHEN THE SEALING 'O' RING WAS LUBRICATED, AND THE NOZZLE WAS CHAMFERED IN ACCORDANCE WITH THE MANUFACTURERS SERVICE BULLETIN, THE EXTINGUISHER NOZZLE FIT THROUGH THE SEALING 'O' RING EASILY AND NO LEAKAGE OCCURRED.

Probable Cause: A malfunction of the cargo fire warning system which resulted in a false alarm.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC93IA113
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB NYC93IA113

Revision history:

Date/timeContributorUpdates
17-Mar-2024 15:32 ASN Update Bot Added

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