ASN Wikibase Occurrence # 362352
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 6 March 1993 |
Time: | 21:15 LT |
Type: | Beechcraft A36 |
Owner/operator: | Centerline Aviation, Inc. |
Registration: | N6088S |
MSN: | E-785 |
Year of manufacture: | 1975 |
Total airframe hrs: | 4649 hours |
Engine model: | CONTINENTAL IO-520-BA |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Plano, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Mt. Pleasant, TX (MSA |
Destination airport: | Addison, TX (KADS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT HAD FLOWN APPROXIMATELY 2.65 HOURS AND WAS RETURNING TO THE AIRPORT WHERE HE HAD RENTED THE AIRPLANE WHEN A POWER LOSS OCCURRED. HE STATED THAT HE SWITCHED FUEL TANKS AND THE ENGINE MOMENTARILY RESTARTED THEN QUIT AGAIN. THE AIRPLANE'S RECORDED ALTITUDE WAS 2,500 FEET MEAN SEA LEVEL WHEN THE ENGINE STOPPED. DURING THE EMERGENCY DESCENT HE MANEUVERED OVER POWERLINES THEN LANDED IN AN OPEN FIELD. THE AIRPLANE STRUCK A DIRT MOUND AND A CEMENT CULVERT. THE LEFT FUEL TANK WAS FOUND EMPTY. THE RIGHT FUEL TANK WAS FULL, BUT LEAKED DURING THE NIGHT UNTIL THE RECOVERY TEAM ARRIVED. ELEVEN GALLONS OF FUEL WAS DRAINED FROM THE RIGHT TANK. THE ENGINE WAS TEST RUN USING THE FUEL FROM THE RIGHT TANK. NO ANOMALIES WERE NOTED TO THE ENGINE. DARK NIGHT CONDITIONS PREVAILED
Probable Cause: FUEL STARVATION INDUCED POWER LOSS RESULTANT FROM FAILURE OF THE PILOT TO SWITCH THE FUEL SELECTOR TO THE PROPER FUEL TANK. FACTORS WERE THE DARK NIGHT CONDITIONS AND LACK OF SUITABLE TERRAIN FOR A FORCED LANDING
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW93LA097 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB FTW93LA097
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
17-Mar-2024 20:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation