ASN Wikibase Occurrence # 362460
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 2 February 1993 |
Time: | 21:20 LT |
Type: | Piper PA-28-161 |
Owner/operator: | Blue Bird Aviation |
Registration: | N233PA |
MSN: | 28-7816676 |
Year of manufacture: | 1978 |
Engine model: | LYCOMING O-320-D3G |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Danbury, CT -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | (KDXR) |
Destination airport: | (KDXR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THIS WAS THE FIRST FLIGHT OF THE DAY AND THE TEMPERATURE WAS BELOW FREEZING. THE PILOT PRIMED THE ENGINE SEVERAL TIMES AND THEN ATTEMPTED TO START THE ENGINE. IT RAN FOR A FEW SECONDS AND THEN STOPPED. HE PRIMED IT SEVERAL TIMES AGAIN AND THEN ATTEMPTED ANOTHER START. AGAIN THE ENGINE STARTED AND THEN STOPPED. HE THEN NOTICED A GLOW ON THE GROUND AND EVACUATED THE PASSENGERS WHILE HE ATTEMPTED TO CRANK THE ENGINE, HOWEVER THE FLAMES SPREAD, AND THE PILOT EVACUATED THE AIRPLANE. THE MASTER SWITCH, ELECTRIC FUEL PUMP, MIXTURE CONTROL AND THE FUEL SELECTOR VALVE WERE LEFT ON. ACCORDING TO THE AIRPLANE FLIGHT MANUAL, PRIMING IS USED ONLY AFTER THE INITIAL START ATTEMPT. IN ADDITION, IF A FIRE OCCURS DURING START, THE MANUAL SAY TO SHUT OFF THE MIXTURE AND FUEL SELECTOR. THE PILOT HAD 90 HOURS TOTAL TIME.
Probable Cause: THE PILOT'S IMPROPER EMERGENCY PROCEDURES FOR AN ENGINE FIRE DURING STARTING WHICH RESULTED IN THE SUBSTANTIAL DAMAGE. FACTORS RELATED TO THE ACCIDENT WERE THE PILOT'S IMPROPER STARTING PROCEDURE AND HIS LACK OF TOTAL EXPERIENCE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC93LA060 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB NYC93LA060
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
18-Mar-2024 06:40 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation