Accident Glasair III N115DM,
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ASN Wikibase Occurrence # 363846
 
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Date:Friday 10 April 1992
Time:08:30 LT
Type:Silhouette image of generic GLAS model; specific model in this crash may look slightly different    
Glasair III
Owner/operator:Rothweiler, Charles
Registration: N115DM
MSN: 3029
Total airframe hrs:127 hours
Engine model:LYCOMING IO-540-K
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Casa Grande, AZ -   United States of America
Phase: En route
Nature:Private
Departure airport:Chandler, AZ (P10)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT WAS ON A PERSONAL CROSS COUNTRY FLIGHT TO A NEARBY AIRPORT. ABOUT 30 MINUTES AFTER TAKEOFF, THE ENGINE SUDDENLY QUIT. EMERGENCY PROCEDURES, INCLUDING ROTATION OF THE FUEL SELECTOR HANDLE, FAILED TO RESTART THE ENGINE AND A FORCED LANDING AREA WAS SELECTED ON A RURAL DIRT ROAD. AS THE PILOT WAS PREPARING TO LAND, A SCHOOL BUS OCCUPIED THE LANDING ZONE, AND THE PILOT THEN SELECTED AN ADJACENT ROAD. DURING THE LANDING, THE LEFT WING STRUCK TREES LOCATED ALONG THE SIDE OF THE ROAD. FAA PERSONNEL REPORTED THAT THE FUEL SELECTOR WAS IN THE OFF POSITION, BUT PLACARDED AS THE MAIN TANK POSITION. THE AIRPLANE'S MAIN WING FUEL TANKS CONTAINED FUEL; HOWEVER A HEADER TANK WAS EMPTY. MAINTENANCE PERSONNEL REPORTED THAT ON THE EVENING PRIOR TO DEPARTURE, THE FUEL SELECTOR WAS POSITIONED ON THE HEADER TANK, WHICH HAS A CAPACITY OF ABOUT 5 GALLONS. THE PILOT, WHO HAS ABOUT 10 HOURS OF EXPERIENCE IN THE AIRPLANE, DID NOT REMEMBER WHAT FUEL TANK WAS SELECTED. AFTER THE ACCIDENT, THE MANUFACTURER ISSUED A MANDATORY SERVICE BULLETIN REQUIRING A PLACARD DETAILING THE FUEL HANDLE POSITIONS, AND INSTALLATION OF MECHANICAL STOPS AND A MOVABLE GATE TO PRECLUDE INADVERTENT SELECTION OF THE OFF POSITION.

Probable Cause: A FAILURE OF THE PILOT TO SELECT THE PROPER FUEL TANK AND SUBSEQUENT FUEL STARVATION. CONTRIBUTING TO THE ACCIDENT WAS AN INADEQUATE DESIGN BY THE MANUFACTURER THAT PERMITTED THE FUEL SELECTOR TO BE ROTATED 360 DEGREES, AND THE PILOT'S LACK OF FAMILIARITY WITH THE AIRPLANE.

Accident investigation:
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Investigating agency: NTSB
Report number: LAX92LA176
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB LAX92LA176

Revision history:

Date/timeContributorUpdates
19-Mar-2024 06:44 ASN Update Bot Added

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