Accident Beechcraft 58 Baron N4188S,
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ASN Wikibase Occurrence # 364083
 
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Date:Sunday 12 January 1992
Time:18:15 LT
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Beco Aviation, Inc.
Registration: N4188S
MSN: TH-620
Year of manufacture:1975
Total airframe hrs:5192 hours
Engine model:CONTINENTAL IO-520C
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:West Palm Beach, FL -   United States of America
Phase: Approach
Nature:Private
Departure airport:Marsh Harbour, OF
Destination airport:Fort Pierce, FL (KFPR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
AFTER ARRIVING IN THE TRAFFIC PATTERN OF THE DESTINATION ARPT, THE PLT LOWERED THE LANDING GEAR SELECTOR HANDLE BUT THE GEAR DID NOT EXTEND. THE FLT DEPARTED THE PATTERN & ATTEMPTS TO LOWER THE GEAR VIA THE EMERGENCY METHOD WERE UNSUCCESSFUL. THE FLT DIVERTED TO A LARGER ARPT WHERE A GEAR UP LANDING OCCURRED. THE LANDING GEAR RETRACT MOTOR & GEARBOX ASSY WAS REMOVED FROM THE ACFT & DISASSEMBLY REVEALED THAT THE WORM SECTOR GEAR REPEATEDLY CONTACTED THE SECTOR GEAR STOP. ALSO, TWO HALF RINGS WHICH SECURE THE BEARING TO THE WORM ACTUATING SHAFT SHEARED. THIS ALLOWED THE WORM GEAR ACTUATOR TO TRAVEL TOWARD THE MOTOR. AS A RESULT, THE HAND CRANK ENGAGING SHAFT WOULD NOT CONTACT THE WORM GEAR ACTUATOR. ACCORDING TO A MECHANIC, THIS WAS DUE TO A WORN LANDING GEAR MOTOR WHICH WOULD DRIVE THE GEAR BUT WOULD RENDER THE DYNAMIC BRAKING ACTION INOPERATIVE. THE UP-LIMIT SWITCH WAS TESTED & FOUND TO OPERATE NORMALLY.

Probable Cause: PARTIAL FAILURE OF THE LANDING GEAR MOTOR WHICH CAUSED INTERNAL DAMAGE TO THE LANDING GEAR RETRACT MOTOR AND GEARBOX ASSY.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA92LA063
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB MIA92LA063

Location

Revision history:

Date/timeContributorUpdates
19-Mar-2024 09:12 ASN Update Bot Added

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