Serious incident de Havilland Canada DHC-8-102 N923HA,
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ASN Wikibase Occurrence # 364084
 
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Date:Sunday 12 January 1992
Time:16:18 LT
Type:Silhouette image of generic DH8A model; specific model in this crash may look slightly different    
de Havilland Canada DHC-8-102
Owner/operator:USAir Express
Registration: N923HA
MSN: 99
Total airframe hrs:9965 hours
Engine model:P&W PW120A
Fatalities:Fatalities: 0 / Occupants: 33
Aircraft damage: Minor
Category:Serious incident
Location:Baltimore, MD -   United States of America
Phase: Initial climb
Nature:Unknown
Departure airport:
Destination airport:Charlottesville, VA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
AS THE GEAR & FLAPS WERE RETRACTED AFTER TAKEOFF, THE #1 ENGINE LOW FUEL PRESSURE WARNING LIGHT ILLUMINATED. AT ABOUT 400' AGL, A "LOUD BANG" WAS HEARD FOLLOWED BY A #1 ENGINE FIRE WARNING INDICATION. THE ENGINE WAS SHUT DOWN & BOTH FIRE EXTINGUISHING BOTTLES WERE DISCHARGED. THE FLIGHTCREW EXTENDED THE LANDING GEAR BY USING THE ALTERNATE SYSTEM & MADE A NO-FLAP EMERGENCY LANDING. THEY USED EMERGENCY BRAKES, BUT DIRECTIONAL CONTROL WAS LOST & THE AIRCRAFT EXITED THE SIDE OF THE RUNWAY & STOPPED WITH THE FIRE EXTINGUISHED. AN EXAM OF THE #1 ENGINE AREA REVEALED A FAILED LOW FUEL PRESSURE WARNING SWITCH SNUBBER & FIRE DAMAGE TO THE ENGINE, NACELLE & WHEELWELL. THERE WAS EVIDENCE THAT DURING INSTALLATION, THE LOW FUEL PRESSURE WARNING SWITCH SNUBBER WAS TORSIONALLY DEFORMED, THEN FATIGUE & SUBSEQUENT FAILURE OCCURRED. GAPS IN THE FIREWALL ALLOWED LEAKING FUEL (SPRAY) TO ENTER THE HOT SECTION & IGNITE. THIS RESULTED IN AN EXPLOSION & FIRE. FIRE PROPAGATION RESULTED IN BURNED WIRES TO THE #1 STANDBY HYDRAULIC PUMP & A RUPTERED #2 SYSTEM HYDRAULIC LINE.

Probable Cause: IMPROPER INSTALLATION OF THE LOW FUEL PRESSURE WARNING SWITCH SNUBBER ON THE #1 ENGINE, RESULTING IN FATIGUE FAILURE OF THE SNUBBER, A FUEL LEAK (SPRAY), AND SUBSEQUENT EXPLOSION/FIRE DAMAGE. A FACTOR RELATED TO THE INCIDENT WAS: INADEQUATE DESIGN OF THE FIREWALL, WHICH ALLOWED FUEL VAPORS TO MIGRATE TO THE HOT SECTION OF THE ENGINE.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: BFO92IA017
Status: Investigation completed
Duration: 3 years and 2 months
Download report: Final report

Sources:

NTSB BFO92IA017

Location

Revision history:

Date/timeContributorUpdates
19-Mar-2024 09:17 ASN Update Bot Added

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