ASN Wikibase Occurrence # 364091
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 11 January 1992 |
Time: | 16:10 LT |
Type: | Beechcraft A36 |
Owner/operator: | Private |
Registration: | N15PM |
MSN: | E-1016 |
Year of manufacture: | 1977 |
Engine model: | CONTINENTAL IO-520-BA |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Griffith, IN -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE PRACTICING TAKE OFFS AND LANDINGS, THE PILOT INADVERTENTLY RETRACTED THE LANDING GEAR PRIOR TO POSITIVE LIFT OFF. THE ACFT SETTLED ON THE RUNWAY AND SLID OFF THE END OF THE RUNWAY.
Probable Cause: PREMATURE GEAR RETRACTION DURING TAKEOFF ROLL BY THE PILOT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI92LA072 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB CHI92LA072
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 09:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation