ASN Wikibase Occurrence # 36417
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Date: | Thursday 8 December 1994 |
Time: | 22:38 LT |
Type: | Beechcraft E18S |
Owner/operator: | Cape Central Airways |
Registration: | N5647D |
MSN: | BA364 |
Engine model: | P&W R-985-AN-14B |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Kansas City, MO -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Sedalia, MO (KDMO) |
Destination airport: | (KMCI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING ARRIVAL AT NIGHT IN FOG AND DRIZZLE, THE PILOT WAS CLEARED FOR AN ILS RUNWAY 1L APPROACH. WHILE ON THE APPROACH, SHE REPORTED ENCOUNTERING MODERATE RIME ICE. RADAR DATA SHOWED THAT THE AIRPLANE CONTINUED INBOUND ON THE LOCALIZER UNTIL IT NEARED THE MIDDLE MARKER, THEN IT DEVIATED ABOUT 20 DEGREES LEFT AND COLLIDED WITH THE GROUND, ABOUT 300' SHORT AND 300' LEFT OF THE THRESHOLD. ACCORDING TO WITNESSES, THE AIRPLANE STOPPED ITS DESCENT AND SLOWED DOWN, SHORTLY BEFORE ENTERING A STEEP DESCENT AND A SPIN. AN ON-SCENE INVESTIGATION REVEALED NO PREIMPACT AIRFRAME, CONTROL SYSTEM, OR POWERPLANT ANOMALIES. THE WINGS HAD 1/4 INCH OF ICE ON THE LEADING EDGE AND A 1/2 INCH HIGH RIDGE OF ICE, PARALLEL TO THE DEICING BOOTS, ABOUT 3 INCHES AFT OF THE BOOTS. THE COCKPIT AND WINDSHIELD HEATING SYSTEM WERE FOUND IN THE 'OFF' POSITION. THE PILOT'S LOGBOOK WAS NOT AVAILABLE FOR INSPECTION. COMPANY RECORDS SHOWED SHE HAD PASSED A 14 CFR PART 135 CHECKRIDE ON MAY 20, 1994. THE FAA CHECKRIDE FORM WAS ADMINISTERED AND SIGNED BY THE CHIEF PILOT. HOWEVER, OTHER RECORDS/INFORMATION SHOWED THE CHIEF PILOT WOULD NOT HAVE BEEN ABLE TO HAVE GIVEN THE CHECKRIDE ON THAT DATE.
Probable Cause: FAILURE OF THE PILOT TO MAINTAIN ADEQUATE AIRSPEED ON FINAL APPROACH, WHICH RESULTED IN AN INADVERTENT STALL/SPIN. FACTORS RELATED TO THE ACCIDENT WERE: THE ADVERSE WEATHER (ICING) CONDITIONS, THE ACCUMULATION OF AIRFRAME/WING ICE, THE PILOT'S IMPROPER USE OF THE ANTI-ICE/DEICE EQUIPMENT, INADEQUATE TRAINING OF THE PILOT CONCERNING FLIGHT IN ICING CONDITIONS, AND INADEQUATE SURVEILLANCE OF THE OPERATION BY THE CHIEF PILOT (COMPANY/OPERATOR MANAGEMENT).
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI95LA053 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI95LA053
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 17:55 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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