ASN Wikibase Occurrence # 364202
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 1 December 1991 |
Time: | 16:56 LT |
Type: | Cessna 210 |
Owner/operator: | Private |
Registration: | N9503T |
MSN: | 210-57303 |
Total airframe hrs: | 2810 hours |
Engine model: | CONTINENTAL IO-470-E |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Groves, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Cartersville, GA (6A0 |
Destination airport: | Houston, TX (KAXH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACCORDING TO THE PILOT, HE ENCOUNTERED THE FORECAST HEAD WINDS EN ROUTE AND HE INTENTIONALLY RAN THE LEFT TANK DRY AND WAS FLYING ON THE RIGHT TANK DURING THE DESCENT WHEN IT ALSO RAN DRY. HE STATED THAT AT THE TIME OF THE TANK CHANGE HE THOUGHT ABOUT REQUESTING AN ALTERNATE, BUT DID NOT. AFTER THE ENGINE FAILURE THE PILOT WAS GIVEN RADAR VECTORS TO THE FINAL LOCALIZER APPROACH COURSE OF A NEARBY AIRPORT; HOWEVER, HE HAD INSUFFICIENT ALTITUDE TO REACH THE RUNWAY. HE BROKE OUT AT 700 FEET AND WAS ABLE TO LAND ON A PLAYING FIELD ADJACENT TO A CHURCH IN AN URBAN AREA. AFTER ROLLING ABOUT 234 FEET, THE AIRPLANE STRUCK A BASEBALL BACK STOP AND CAME TO REST IN THE CHURCH PARKING LOT. THE PILOT'S FUEL CALCULATIONS INDICATED THAT HE HAD 6.5 HOURS TO FUEL EXHAUSTION, WHILE ACTUAL FUEL EXHAUSTION OCCURRED AFTER 5.5 HOURS. THE LEFT TANK RAN DRY AT 2.6 HOURS AND THE RIGHT RAN DRY AT 2.9 HOURS.
Probable Cause: FUEL EXHAUSTION WHICH PRECIPITATED THE FORCED LANDING DUE TO THE PILOT'S INADEQUATE FUEL CONSUMPTION CALCULATIONS. A FACTOR IN THE ACCIDENT WAS THE PILOT'S FAILURE TO DIVERT TO AN ALTERNATE DESTINATION WHEN HE RECOGNIZED THAT FUEL EXHAUSTION WAS A POSSIBILITY.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW92LA031 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW92LA031
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 12:37 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation