ASN Wikibase Occurrence # 364222
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Date: | Tuesday 26 November 1991 |
Time: | 15:01 LT |
Type: | Cessna 182H |
Owner/operator: | Snoopy's Flight School |
Registration: | N1986X |
MSN: | 18256086 |
Year of manufacture: | 1965 |
Engine model: | CONTINENTAL O-470-U |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tucson, AZ -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | El Paso, TX (KELP) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID THAT PRIOR TO DEPARTURE AT EL PASO SHE VISUALLY LOOKED IN EACH FUEL TANK AND ESTIMATED THEY WERE TWO THIRDS FULL. SHE DID NOT PHYSICALLY MEASURE THE FUEL QUANTITY. THE LEFT FUEL GAGE WAS KNOWN TO BE INOPERATIVE BY THE PILOT. ON A TWO MILE FINAL APPROACH TO TUCSON THE ENGINE BEGAN TO SPUTTER. THE PILOT SWITCHED FUEL TANKS AND THE ENGINE QUIT. THE AIRCRAFT COLLIDED WITH ROUGH TERRAIN DURING THE SUBSEQUENT FORCED LANDING ATTEMPT IN A DESERT AREA EAST OF THE TUCSON AIRPORT. THE AIRCRAFT WAS EXAMINED BY FAA INSPECTORS. THE LEFT FUEL TANK WAS COMPLETELY DRY AND THE RIGHT TANK CONTAINED ONLY RESIDUAL FUEL. FUEL SYSTEM CONTINUITY WAS ESTABLISHED. THE FAA INSPECTORS REPORTED THAT THE OPERATOR KNEW ABOUT THE INOPERATIVE FUEL GAGE PRIOR TO THIS FLIGHT BUT DID NOT REPAIR IT DURING THE LAST MAINTENANCE PERIOD. AN OPERATIVE FUEL QUANTITY INDICATING SYSTEM IS REQUIRED BY REGULATION FOR FLIGHT.
Probable Cause: FUEL EXHAUSTION DUE TO THE PILOT'S INADEQUATE PREFLIGHT INSPECTION, HER FAILURE TO ENSURE THAT AN ADEQUATE FUEL SUPPLY WAS ONBOARD AND HER DECISION NOT TO REFUEL THE AIRCRAFT PRIOR TO DEPARTURE. FACTORS IN THE ACCIDENT WERE: 1) THE INOPERATIVE LEFT FUEL GAGE; 2) THE FAILURE OF THE OPERATOR MANAGEMENT TO ADEQUATELY MAINTAIN THE AIRCRAFT AND 3) THE PILOT'S DECISION TO OPERATE THE AIRCRAFT WITH KNOWN DEFICIENCIES IN THE REQUIRED EQUIPMENT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX92LA059 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB LAX92LA059
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 12:50 |
ASN Update Bot |
Added |
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