ASN Wikibase Occurrence # 364237
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Date: | Wednesday 20 November 1991 |
Time: | 11:32 LT |
Type: | Mcdonnell Douglas MD-88 |
Owner/operator: | Delta Air Lines |
Registration: | N908DL |
MSN: | 49539/1366 |
Total airframe hrs: | 12637 hours |
Engine model: | P&W JT8D-219 |
Fatalities: | Fatalities: 0 / Occupants: 29 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Atlanta, GA -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Atlanta, GA (KATL) |
Destination airport: | Montgomery, AL |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER LIFTOFF A PASSENGER IN ROW 18 REPORTED OBSERVING FLAMES COMING FROM THE OVERHEAD AREA ON THE RIGHT SIDE OF THE AIRPLANE. THE FLIGHT ATTENDANT SUPPRESSED THE REPORTED AREA WITH A HALON FIRE EXTINGUISHER AND REPORTED THE INCIDENT TO THE FLIGHT DECK. HOWEVER, THE FLIGHT ATTENDANT DID NOT REPORT SEEING FLAMES. AN EMERGENCY LANDING WAS MADE AT THE DEPARTURE AIRPORT WITHOUT FURTHER INCIDENT. EXAMINATION OF THE OVERHEAD AREA AROUND ROW 18 REVEALED THAT THE CANNON PLUG CONNECTOR ADJACENT TO THE LIGHT ASSEMBLY HAD SHORTED. SUBSEQUENT EXAMINATIONS OF THE CONNECTOR REVEALED THAT PINS IN THE MATING HALVES OF THE CONNECTOR WERE DAMAGED, AND APPEARED TO HAVE OCCURED WHEN A PREVIOUS CONNECTION WAS ATTEMPTED. RESEARCH EFFORTS TO DUPLICATE THE CONNECTOR FAILURE MODE FAILED. A REVIEW OF THE OPERATORS MAINTENANCE RECORDS FAILED TO DISCLOSE IF ANY MAINTANANCE HAD BEEN CONDUCTED IN THE AREA OF THE CONNECTOR. HOWEVER, THE OPERATOR COULD NOT VERIFY THAT THE CONNECTOR AND AFFECTED AREAS WERE NEVER SERVICED DURING A PREVIOUS STOPOVER
Probable Cause: A SHORT IN AN ELECTRICAL CONNECTOR WHICH RESULTED IN ITS FAILURE. THE REASON FOR THE SHORT WAS NOT DETERMINED. A FACTOR WAS THE IMPROPER INSTALLATION OF THE CONNECTOR BY AN UNKNOWN MAINTENANCE PERSON.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL92IA025 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ATL92IA025
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 13:03 |
ASN Update Bot |
Added |
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