Accident Beechcraft D18S N4193,
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ASN Wikibase Occurrence # 364258
 
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Date:Sunday 10 November 1991
Time:09:50 LT
Type:Silhouette image of generic BE18 model; specific model in this crash may look slightly different    
Beechcraft D18S
Owner/operator:Tomy International
Registration: N4193
MSN: A980
Total airframe hrs:19936 hours
Engine model:P&W R-985-AN14B
Fatalities:Fatalities: 0 / Occupants: 11
Aircraft damage: Substantial
Category:Accident
Location:Hilo, HI -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Honolulu, HI (HNL)
Destination airport:Hilo, HI (ITO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
ABT 45 MI FM LNDG, THE L ENG RPM BGN TO FLUCTUATE, THEN AT ABT 15 MI FM LNDO, IT LOST POWER ALTOGETHER. THE PLT SAID THE ACFT WOULD NOT MAINT ALTITUDE. UNABLE TO RCH THE RWY, HE DITCHED THE ACFT IN HILO BAY ABT 1/4 MI FM SHORE & 1.5 MI FM THE ARPT. AFTER RETRIEVAL, THE ACFT & L ENG WERE EXAMINED. THE ACCESSORY GEAR DRIVE SHAFT WAS FND TO HAVE FAILED IN TORSIONAL OVERLOAD. ON THE INSIDE OF THE CASE, AN AREA OF GOUGING & ABRASION WAS FND DRCTLY IN FNT OF THE STARTER GEAR. (THE LEFT MAG, FUEL PUMP & PROP GOVERNOR WERE DRIVEN BY THE ACCESSORY DRIVE GEAR.) DEEP IMPRESSIONS WERE NOTED ON ABT 70% OF THE GEAR TEETH, WITH MTRL DISPLACEMENT & GOUGING EVIDENT. THERE WAS EVIDENCE THAT THE COLLECTOR DRIVE FLOATING GEAR MAY HAVE MOVED FORWARD & HAD CONTACTED THE ENG CASE. ALSO, THERE WAS EVIDENCE OF MECHANICAL INTERFERENCE WITHIN THE ACCESSORY DRIVE GEAR SYS. THE ACFT GROSS WT AT THE TIME OF THE ACDNT WAS ABOUT 9108 LBS.

Probable Cause: THE AIRCRAFT'S LACK OF SINGLE ENGINE PERFORMANCE TO MAINTAIN ALTITUDE AFTER THE ENGINE LOST POWER. FACTORS RELATED TO THE ACCIDENT WERE: DISPLACEMENT/MECHANICAL INTERFERENCE WITHIN THE ACCESSORY DRIVE GEAR SYSTEM OF THE LEFT ENGINE, FAILURE OF THE LEFT ENGINE ACCESSORY DRIVE GEAR SHAFT, AND THE FAA'S INADEQUATE CERTIFICATION/APPROVAL OF THE OPERATOR, IN ORDER TO ASSURE COMPLIANCE WITH 14 CFR 135 CONCERNING THE ENGINE-OUT CAPABILITY.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX92LA042
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB LAX92LA042

Location

Revision history:

Date/timeContributorUpdates
19-Mar-2024 13:16 ASN Update Bot Added

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