ASN Wikibase Occurrence # 364366
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Date: | Tuesday 15 October 1991 |
Time: | 16:55 LT |
Type: | Piper PA-18 |
Owner/operator: | Private |
Registration: | N3850Z |
MSN: | 18-7608 |
Year of manufacture: | 1961 |
Total airframe hrs: | 1653 hours |
Engine model: | LYCOMING O-320-B2B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Montague Island, AK -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Cordova, AK (CDV) |
Destination airport: | Cordova, AK (CDV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING CRUISE FLIGHT, THE ENGINE SEIZED WITHOUT WARNING. WITH NO SUITABLE LANDING AREA ON THE BEACH, THE PILOT DITCHED IN THE OCEAN AND SWAM ASHORE ABOUT 1/2 MILE AWAY. AN INVESTIGATION REVEALED THAT THE CRANKSHAFT HAD BROKEN AT THE FORWARD CHEEK OF THE #3 MAIN BEARING. A REDDISH SEALANT RESIDUE WAS FOUND AROUND THE MAIN BEARING THRU STUD HOLES OF THE CRANKCASE. ACCORDING TO LYCOMING SERVICE INSTRUCTION #1125A, SEALANT SHOULD NOT HAVE BEEN APPLIED IN THIS AREA.
Probable Cause: THE POWER LOSS DUE TO THE CRANKSHAFT FAILURE. CONTRIBUTING TO THE ACCIDENT WAS IMPROPER MAINTENANCE DURING THE LAST ENGINE OVERHAUL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC92FA005 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB ANC92FA005
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 14:15 |
ASN Update Bot |
Added |
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