ASN Wikibase Occurrence # 364416
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 6 October 1991 |
Time: | 16:16 LT |
Type: | Cessna 320 |
Owner/operator: | Private |
Registration: | N4726X |
MSN: | 3200026 |
Engine model: | CONTINENTAL TSIO-520B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gadsden, AL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Panama City, FL (KPFN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT WAS AWARE OF A PROBLEM WITH THE AIRCRAFT FUEL SYSTEM, SINCE FUEL FROM THE RIGHT MAIN TANK WOULD FEED QUICKER THAN FROM THE LEFT MAIN TANK. RATHER THAN HAVE THE A/C REPAIRED IN FLORIDA, HE ELECTED TO FLY THE A/C TO HIS HOME IN INDIANA TO HAVE THE REPAIRS DONE THERE. WHILE ON APPROACH TO A REFUELING STOP, HE REPORTED THAT BOTH ENGINES QUIT SIMULTANEOUSLY. A FORCED LANDING WAS MADE IN A NEARBY FIELD. THE INVESTIGATION REVEALED THAT THE LT TANK BOOST PUMP WAS INOP, AND THE FUEL SYSTEM CROSSFEED LINES WERE INCORRECTLY INSTALLED (NORMAL X-FEED WAS DISABLED). THUS, FUEL FROM THE RT, MAIN TANK WAS PRESSURE FED TO THE LT, MAIN TANK, AND THEN OVERBOARD, UNTIL THE RT TANK WAS EMPTIED, AND THE RT ENGINE QUIT. HOWEVER, FUEL WAS STILL AVAILABLE TO THE LT ENGINE. THEREFORE THE SAFETY BOARD BELIEVES THAT THE PILOT SELECTED X-FEED ON THE LT FUEL SELECTOR AFTER THE RT ENGINE QUIT; THIS SUBSEQUENTLY SHUT OFF FUEL TO THE LT ENGINE.
Probable Cause: FUEL STARVATION DUE TO INCORRECT FUEL LINE INSTALLATIONS, AN INOPERATIVE FUEL BOOST PUMP, AND INCORRECT PILOT PROCEDURE. A FACTOR IN THIS ACCIDENT WAS THE PILOT'S INTENTIONAL OPERATION WITH A KNOWN FUEL SYSTEM DEFICIENCY.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL92LA003 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB ATL92LA003
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 14:48 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation