ASN Wikibase Occurrence # 364817
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 28 July 1991 |
Time: | 15:50 LT |
Type: | Beechcraft C23 |
Owner/operator: | Private |
Registration: | N7690R |
MSN: | M1290 |
Total airframe hrs: | 2096 hours |
Engine model: | LYCOMING O-360-A2G |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Williamstown, MA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Bennington, VT (5BE) |
Destination airport: | Gt. Barrington, MA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A 200 HOUR PRIVATE PILOT EXPERIENCED A COMPLETE LOSS OF ENGINE POWER WHILE IN CRUISE FLIGHT AT 3,000 FEET. THE ENGINE FAILURE WAS THE RESULT OF THE CRANKSHAFT GEAR RETAINING BOLT BACKING OUT RESULTING IN THE DISENGAGEMENT OF THE CRANKSHAFT. THE ENGINE HAD RECENTLY BEEN OVERHAULED, BUT THE MANUFACTURER'S SERVICE INSTRUCTIONS WERE NOT COMPLIED WITH AT THE TIME OF THE ENGINE OVERHAUL. SUITABLE TERRAIN WAS NOT AVAILABLE TO THE PILOT TO EXECUTE A SUCCESSFUL FORCED LANDING.
Probable Cause: ENGINE FAILURE AS A RESULT OF IMPROPER ENGINE OVERHAUL PERFORMED BY OTHER MAINTENANCE PERSONNEL. A FACTOR WAS THE LACK OF SUITABLE TERRAIN.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC91LA191 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB NYC91LA191
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 19:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation