Accident Piper PA-32R-301T Turbo Saratoga SP N43515,
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ASN Wikibase Occurrence # 36527
 
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Date:Wednesday 11 July 1990
Time:02:21
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-301T Turbo Saratoga SP
Owner/operator:Executive Protection
Registration: N43515
MSN: 32R-8429009
Year of manufacture:1984
Engine model:LYCOMING TIO-540-S1AD
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Ashton, IL -   United States of America
Phase: En route
Nature:Private
Departure airport:Chicago, IL (MDW)
Destination airport:Lincoln, NE (LNK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE FLT ORIGINATED AT 0151 CDT AFTER THE PLT & PSGR HAD SPENT A DAY SIGHTSEEING & ATTENDED A NGT BASEBALL GAME. BEFORE DEPG, THE PLT RCVD A WX BRIEFING & FILED AN IFR FLT PLAN. OVC SKIES WITH CUMULIFORM CLOUDS & RAIN SHOWERS PREVAILED ALONG THE ROUTE. THOUGH THE PLT WAS NOT BRIEFED ABOUT TSTMS, ONLY WIDELY SCATTERED TSTMS WITH MODERATE RAINSHOWERS WERE FORECAST. WHILE EN ROUTE, THE PLT MADE A TRANSMISSION THAT HIS COMPASS WAS 'SWINGING' & THEN CONTACT WITH THE ACFT WAS LOST. SUBSEQUENLTY, AN INFLT BREAKUP OF THE ACFT OCCURRED & WRECKAGE WAS SCATTERED OVER A WIDE AREA. RADAR DATA SHOWED THAT THE AIRPLANE MADE RAPID CHANGES IN ALTITUDE BEFORE BREAKING UP. AN EXAM OF THE WRECKAGE SHOWED THAT BOTH WINGS FAILED IN POSITIVE OVERLOAD. THE STABILATOR FAILED DOWN & WAS BENT AFT BEFORE SEPARATING FROM THE ACFT. THE REST OF THE AIRCRAFT WAS EXTENSIVELY DAMAGED BY IMPACT & FIRE.

CAUSE: A LOSS OF AIRCRAFT CONTROL FOR AN UNKNOWN REASON, WHILE EN ROUTE IN INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) ON A DARK NIGHT, AND THE PILOT EXCEEDING THE DESIGN STRESS LIMITS OF THE AIRCRAFT WHILE ATTEMPTING TO RECOVER FROM UNCONTROLLED FLIGHT. FACTORS RELATED TO THE ACCIDENT WERE: PILOT FATIGUE AND PROBABLE SPATIAL DISORIENTATION OF THE PILOT AND/OR AN INSTRUMENT MALFUNCTION.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI90FA174
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
17-May-2022 13:45 harro Updated [Aircraft type, Source, Narrative, Accident report]

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