ASN Wikibase Occurrence # 36568
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Date: | Friday 10 December 1993 |
Time: | 20:05 LT |
Type: | Bellanca 17-30A Super Viking 300A |
Owner/operator: | Adamson, Seabron C. |
Registration: | N4195B |
MSN: | 74-30725 |
Total airframe hrs: | 1768 hours |
Engine model: | CONTINENTAL IO-520K |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Lagrange, GA -
United States of America
|
Phase: | Approach |
Nature: | Executive |
Departure airport: | Brunswick, GA (KBQK) |
Destination airport: | (KLGC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:MOMENTS BEFORE THE FLIGHT DEPARTED, THE PILOT REQUESTED AN ENGINE JUMP START FROM THE LOCAL FIXED BASE OPERATOR. HE TOLD THE MAINTENANCE PERSON THAT HE LEFT THE LORAN ON AND THE BATTERY WAS COMPLETLEY DRAINED. THE MAINTENANCE PERSON URGED THE PILOT TO CHARGE THE BATTERY BEFORE STARTING THE TRIP, BUT THE PILOT SAID, HE HAD AN IMPORTANT MEETING AND MUST RETURN. ALL AIR TRAFFIC CONTROL HANDLING WAS NORMAL. ACCORDING TO THE APPROACH CONTROLLER, THE FLIGHT'S PROFILE APPEARED NORMAL ON RADAR AND THE PILOT DID NOT REPORT ANY DIFFICULTIES. AS THE FLIGHT CONTINUED THE APPROACH TO LAND, A WITNESS SAW THE AIRPLANE IN SUCH AN ATTITUDE THAT HE COULD SEE THE WHITE PAINTED TOP OF THE AIRPLANE. THE WITNESS SAID, THERE WERE NO LIGHTS ILLUMINATED ON THE AIRPLANE PRIOR TO IT'S IMPACT WITH TH GROUND. EXAMINATION OF THE WRECKAGE FAILED TO DISCLOSE A MECHANICAL PROBLEM. ELECTRICAL COMPONENTS, INCLUDING THE BATTERY, WERE DESTROYED BY IMPACT FORCES. EXAMINATION OF A NAVIGATIONAL LIGHT RECOVERED FROM THE AIRPLANE FAILED TO DISCLOSE ANY UNUSUAL DEFORMATION TO THE BULB FILAMENT. AN EXAMINATION OF FAA RECORDS FAILED TO DISCLOSE AN AIRMAN INSTRUMENT CERTIFICATION FOR THE PILOT.
Probable Cause: WAS THE PILOT'S FAILURE TO CORRECT A KNOWN LOW BATTERY CONDITION BEFORE DEPARTING, WHICH RESULTED IN A LOSS OF ELECTRICAL POWER DURING AN INSTRUMENT APPROACH. FACTORS WERE THE DARK NIGHT AND THE LOW SCATTERED CLOUD LAYER.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL94FA028 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB ATL94FA028
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 09:46 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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