ASN Wikibase Occurrence # 366627
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Date: | Sunday 8 July 1990 |
Time: | 12:36 LT |
Type: | Cessna 404 |
Owner/operator: | U.s. Customs |
Registration: | N6239G |
MSN: | 404-0229 |
Total airframe hrs: | 5885 hours |
Engine model: | CONTINENTAL GTSIO-520-M2 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Angelo, TX -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | (KSJT) |
Destination airport: | (KSJT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:FM 9500' MSL AT 35 DME, COPLT (SIC) BGN (HOODED TYPE) ILS RWY 3 APCH WITH 14 TO 22 KT TAILWIND. HE PLANNED NOT TO EXCEED500'/MIN RATE OF DSCNT TO AVOID SUPERCOOLING ENGS. PIC RPRTD ACFT WAS OFF COURSE & ABT 1500' HI AS IT APCHD OM. HE TOOK CTL & MNVRD ACFT ON COURSE & GP, THEN RTRND CTL TO SIC TO CONT ILS. DRG MNVR, 2500'/MIN DSCNT OCCURRED; SPD INCRD 31 KT.AS APCH CONTD, PIC EXTDD GEAR & FLAPS. AS ACFT SLOWED & BGN SETTLING, SIC ADVND THROTTLES, BUT ENGS DIDN'T RESPOND. PIC TOOK CTL & BOTH PLTS MANIPULATED ENG CTLS, BUT PWR WASN'T RESTORED. RECALLATIONS DIFFERED; NEITHER PLT COULD RECALL ENG INST INDCNS. GEAR COLLAPSED AS ACFT CTCD GND SHORT OF RWY & SLID THRU FENCE. MIX CTLS WERE FND ABT 4 TO 5 'CLICKS' AFT OF FULL FWD PSN, THROTTLES FND AT ABT 3/4 FWD PSN; ABT 80 GAL OF FUEL FND IN WING TANKS. INV REVEALED SERIES OF MAINT WRITE-UPS NOTING ENGS HAD RUN RICH & ROUGH, BUT NO PRE-ACDNT PART FAILURE OR MALFUNCTION WAS FND. ENGS OPNLY CHECKED OK.REAR SEAT PAX THOUGHT PIC PULLED PROP CTLS 'DOWN' & BACK FWD. GND WITNESS RPRTD SOUND AS IF 'PROP REVERSERS REVVED UP.'
Probable Cause: IMPROPER USE OF POWERPLANT CONTROLS BY THE PILOT-IN-COMMAND (PIC). FACTORS RELATED TO THE ACCIDENT WERE: THE PIC'S INADEQUATE CREW COORDINATION, AND THE EXCESSIVE AIRSPEED AND RATE OF DESCENT THAT RESULTED, WHEN THE PIC MANEUVERED THE AIRCRAFT BACK ON COURSE AND GLIDE PATH.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW90GA137 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW90GA137
Revision history:
Date/time | Contributor | Updates |
21-Mar-2024 10:29 |
ASN Update Bot |
Added |
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