ASN Wikibase Occurrence # 366718
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Date: | Monday 25 June 1990 |
Time: | 11:54 LT |
Type: | Spark/acroduster SA/750 |
Owner/operator: | Brian A Donnelly |
Registration: | N10WS |
MSN: | 0015 |
Total airframe hrs: | 176 hours |
Engine model: | LYCOMING IO-360-A1B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Redlands, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT DEPARTED WITH FUEL TANKS HALF FULL FOR SOME ACROBATIC WORK. THE AIRCRAFT WAS AIRBORNE FOR OVER AN HOUR AND 20 MINUTES WHEN THE ENGINE BEGAN TO SPUTTER AFTER A TOUCH AND GO LANDING AND A STEEP CLIMBOUT. ACCORDING TO THE SECOND PILOT ON BOARD THE PILOT STALLED THE AIRCRAFT IN AN ATTEMPT TO RETURN TO THE RUNWAY. WITNESSES ON THE GROUND HEARD THE SPUTTER FROM THE ENGINE AND OBSERVED A TIGHT TURN BACK TO THE RUNWAY. EXAMINATION OF THE WRECKAGE REVEALED NO PRESENCE OF FUEL IN THE TANKS OR FUEL LINES.
Probable Cause: THE PILOTS FAILURE TO MAINTAIN A SPEED ABOVE A STALL AFTER EXPERIENCING A LOSS OF ENGINE POWER. CONTRIBUTING TO THE ACCIDENT WAS THE PILOT'S MISCALCULATION OF THE FUEL SUPPLY.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX90DUG07 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB LAX90DUG07
Location
Revision history:
Date/time | Contributor | Updates |
21-Mar-2024 11:22 |
ASN Update Bot |
Added |
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