ASN Wikibase Occurrence # 366788
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Date: | Friday 15 June 1990 |
Time: | 12:10 LT |
Type: | Ayres S-2R Thrush |
Owner/operator: | Private |
Registration: | N8472V |
MSN: | 2232R |
Total airframe hrs: | 4994 hours |
Engine model: | P&W R1340ANI |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mcgregor, TX -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Mount Pleasant, TX |
Destination airport: | Wharton, TX (5R5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT THE FUEL QUANTITY GAUGE WAS INOPERATIVE AND THAT HE INTENDED TO REFUEL EVERY HOUR AND 45 MINUTES. HE HAD FLOWN FOR TWO HOURS WITHOUT REFUELING ON THE PRECEDING DAY. AT 1,500 FEET THE POWER LOSS OCCURRED. DURING THE FORCED LANDING THE PILOT REALIZED THAT HIS CHOSEN SITE HAD UNEVEN TERRAIN AND DITCHES. HE WAS TRYING TO FLY THE AIRPLANE ACROSS A DITCH WHEN THE TAIL STRUCK THE EMBANKMENT. NO EVIDENCE OF FUEL IN THE WRECKAGE WAS FOUND AND THE SUCCESSFUL ENGINE TEST RUN DID NOT REVEAL ANY MECHANICAL MALFUNCTIONS.
Probable Cause: THE FUEL EXHAUSTION INDUCED POWER LOSS, WHICH RESULTED FROM THE PILOT'S INACCURATE FUEL CONSUMPTION CALCULATIONS.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW90DPA07 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW90DPA07
Location
Revision history:
Date/time | Contributor | Updates |
21-Mar-2024 12:07 |
ASN Update Bot |
Added |
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