ASN Wikibase Occurrence # 366793
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 14 June 1990 |
Time: | 19:00 LT |
Type: | Rockwell S2R |
Owner/operator: | Cartillar Flying Service |
Registration: | N8421V |
MSN: | 2181R |
Year of manufacture: | 1976 |
Engine model: | P&W R-1340-AN1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tilton, AR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Hickory Ridge, AR |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE COMMERCIAL PLT SAID THAT WHILE EN ROUTE TO THE FIELD TO BE TREATED, THE ENGINE BEGAN TO LOSE POWER. AN EMERGENCY LNDG WAS MADE IN A SOFT, WET, FARM FIELD, WHICH RESULTED IN SUBSTANTIAL DAMAGE TO THE ACFT. POST-ACCIDENT INVESTIGATION REVEALED THE ENGINE DRIVEN SUPERCHARGER HAD FAILED.
Probable Cause: FAILURE OF THE ENGINE BLOWER(SUPERCHARGER). RELATED TO THE ACCIDENT WAS THE SOFT/WET TERRAIN, WHERE THE FORCED LANDING WAS PERFORMED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC90LA129 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB MKC90LA129
Location
Revision history:
Date/time | Contributor | Updates |
21-Mar-2024 12:13 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation