ASN Wikibase Occurrence # 367244
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 26 March 1990 |
Time: | 17:45 LT |
Type: | Cessna 150 |
Owner/operator: | Todd's Flying Service Inc. |
Registration: | N2254J |
MSN: | 150-65454 |
Total airframe hrs: | 3856 hours |
Engine model: | CONTINENTAL O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ankeny, IA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Executive |
Departure airport: | (Y42) |
Destination airport: | Lamoni, IA (0Y7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PVT PILOT SAID THAT HE HAD JUST DEPARTED RUNWAY 35 AND HAD TURNED CROSSWIND, WHEN THE ENGINE BEGAN TO SPUTTER. HE MADE A TURN TO RETURN TO THE AIRSTRIP AND LAND ON RUNWAY 17, BUT THE ENGINE LOST POWER, COMPLETELY. UNABLE TO REACH THE PVT AIRSTRIP, AN EMERGENCY LANDING WAS MADE IN A FALLOW CORN FIELD, WHICH RESULTED IN A NOSE OVER. A POST-ACCIDENT INVESTIGATION REVEALED THE FUEL WAS CONTAMINATED WITH WATER.
Probable Cause: FUEL CONTAMINATION AND INADEQUATE AIRCRAFT PREFLIGHT BY THE PILOT IN COMMAND.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC90LA075 |
Status: | Investigation completed |
Duration: | 2 years and 11 months |
Download report: | Final report |
|
Sources:
NTSB MKC90LA075
Location
Revision history:
Date/time | Contributor | Updates |
22-Mar-2024 12:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation